United States Department of Transportation / Federal Aviation Administration logo

AFS-600 Regulatory Support Division logo

 

ADVISORY CIRCULAR

43-16A

 

 

AVIATION MAINTENANCE ALERTS

 

 

flag of the United States of America

 

ALERT

NUMBER

320

bald eagle watching over three eggs

MARCH

2005

 


CONTENTS

AIRPLANES

AIRBUS....................................................................................................................................... 1

CESSNA...................................................................................................................................... 3

LEAR........................................................................................................................................... 3

PIPER........................................................................................................................................... 3

ACCESSORIES

THROTTLE CONTROL CABLE................................................................................................ 4

POWERPLANTS & PROPELLERS

CONTINENTAL......................................................................................................................... 5

GARRETT.................................................................................................................................... 6

HONEYWELL............................................................................................................................. 6

LYCOMING................................................................................................................................ 7

PRATT AND WHITNEY............................................................................................................. 7

ROLLS-ROYCE.......................................................................................................................... 8

TURBOMECA............................................................................................................................. 9

AIR NOTES

ELECTRONIC VERSION OF FAA FORM 8010-4, MALFUNCTION OR
DEFECT REPORT....................................................................................................................... 9

PAPER COPY OF FAA FORM 8010-4, MALFUNCTION OR DEFECT REPORT................. 9

INTERNET SERVICE DIFFICULTY REPORTING (iSDR) WEB SITE................................... 10

IF YOU WANT TO CONTACT US......................................................................................... 11

AVIATION SERVICE DIFFICULTY REPORTS...................................................................... 11

 


U.S. DEPARTMENT OF TRANSPORTATION
FEDERAL AVIATION ADMINISTRATION
WASHINGTON, DC 20590

AVIATION MAINTENANCE ALERTS

The Aviation Maintenance Alerts provide a common communication channel through which the aviation community can economically interchange service experience, cooperating in the improvement of aeronautical product durability, reliability, and safety. This publication is prepared from information submitted by those who operate and maintain civil aeronautical products. The contents include items that have been reported as significant, but have not been evaluated fully by the time the material went to press. As additional facts such as cause and corrective action are identified, the data will be published in subsequent issues of the Alerts. This procedure gives Alerts’ readers prompt notice of conditions reported via a Mechanical Reliability Report (MRR), a Malfunction or Defect Report (M or D), or a Service Difficulty Report (SDR). Your comments and suggestions for improvement are always welcome. Send to: FAA; ATTN: Aviation Data Systems Branch (AFS-620); P.O. Box 25082; Oklahoma City, OK 73125-5029.

(Editor’s notes are provided for editorial clarification and enhancement within an article. They will always be recognized as italicized words bordered by parentheses.)

 

AIRPLANES

AIRBUS

Airbus A330; Main Landing Gear SM9 Pin Retention Bolt

The following is a reprint of an article produced by Transport Canada, Continuing Airworthiness Office, Ottawa, Canada. (The article is published as it was received.)

SERVICE DIFFICULTY ALERT

Airbus A330

Main Landing Gear SM9 Pin Retention Bolt

Transport Canada has been informed, that an Airbus A330 was undergoing heavy maintenance (C2 check) and maintenance personnel discovered the main landing gear oleo upper retention bolt sheared. Transport Canada was informed by an operator, that an Airbus A330 was undergoing a C2 check in preparation for doing a seal change on the right main landing gear.

This item is a crude, black and white close-up photograph showing the steel SM8 bearing pin. Chrome damage is evident.

Pin SM8 UNI 32-10-1337
Chrome Damage (rotated 180o/)


Shown is an expanded view drawing of the upper portion of the R/H main landing gear strut. It demonstrates the part relationship of the SM8 bearing pin and its SM9 retention bolt.

During the disassembly of the right main landing gear for a routine seal change, it was discovered that the SM9 pin retention bolt, CMM 32-12-02-51-50, was had sheared at the bolt head. The bolt, P/N NAS6605D136, retains the pin end caps. One end cap was found on the outer surface of the shock strut assembly. After a detailed examination, further collateral damage on the piston was discovered as well as 50% chrome loss on pin SM8.

The aircraft had accumulated approximately 13,548 flying hours and, 2,372 landings. Based on physical evidence, with the shank of the SM9 pin-retaining pin retaining bolt broke, this allowing the permitted the retaining end cap on the outboard end of the pin to fall off. Unrestrained, the SM8 pin migrated approximately 1" in outboard from its installed position, which is flush with the lower connecting link.

The outboard retaining end cap, with the sheared bolt head, was discovered on the shock strut piston stuck in grease.

Transport Canada strongly recommends operators of this model aircraft inspect the main landing gear retention bolt at their earliest convenience.

Any defects or further occurrences should be reported by sending a Service Difficulty Report to Transport Canada, Continuing Airworthiness, Ottawa.

For further information, contact a Transport Canada Centre, or Mr. Steve Dudka, Continuing Airworthiness, Ottawa, telephone (613) 952-4361, facsimile (613) 996-9178 or e-mail dudkas@tc.gc.ca .

For Director, Aircraft Certification

B. Goyaniuk
Chief, Continuing Airworthiness

Note: For the electronic version of this document, please consult the following Web address:
www.tc.gc.ca/CivilAviation/certification/menu.htm

 

                            Last updated: 2004-12-02                                                 Important Notices

 

Part Total Time:   13,548 hours.

 


CESSNA

Cessna; R182; Broken Rudder Pedal Bearing-Block Support; ATA 5311

A mechanic noticed an unusual “...feeling...” with the aircraft’s rudder pedals during an engine ground-run for a 100-hour inspection. Close observation revealed broken web flanges (P/N 0713628-5 & -6) where nut plates are mounted for attachment of the rudder pedal’s bearing-blocks.

Part Total Time: 5,397.7 hours.

 

LEAR

Lear; 25; Landing Gear Retraction Failure; ATA 3230

The aircraft returned to the airport when the landing gear failed to retract after takeoff. Technicians found the left main gear’s squat switch assembly (P/N 446EN1-9) frozen (locked) in the “ground mode.” A new switch was installed per the Lear 25 service manual and the Dee Howard thrust-reverser manual, bulletins (S/B 25-14B), and letters (SL 38-1).

Part Total Time: (unknown).

 

Lear; 25D; Aircraft Vibration; ATA 2435

The crew reported feeling a vibration in the aircraft during flight. Maintenance determined the right engine’s Bendix starter-generator was causing the problem (P/N 30B37-49B). A serviceable unit was installed and all operational checks were performed per the Learjet 25 maintenance manuals. No diagnostic information was provided.

Part Total Time: (unknown).

 

PIPER

Piper; PA44-180; Cracked Aileron Skin; ATA 5751

An annual inspection found a crack (approximately centered) in an aileron’s outboard skin (P/N 86562-06). The part was replaced. No analysis for the crack’s occurrence was offered. (This mechanic’s report is one of three for similar cracks found in the same location on three different PA44-180 aircraft. Crack descriptions did not include dimensions or a top/bottom aileron reference. The three reported aircraft were all within 327 hours of their respective total times.)

Part Total Time: 7,707.7 hours.

 

Piper; PA44-180; Failure of Stabilator Pitch Control; ATA 2740

This aircraft experienced a complete loss of stabilator control. The lower control cable’s (P/N 62701-153) forward end had corrosion deterioration at the swaged terminal. The mechanic states: “(This) problem is not detectable during periodic inspections per Piper Maintenance Manual, Section 05-21-00, item 29.” He recommends establishing a time life for control cable replacement.

Part Total Time: (unknown).

 


Piper; PA60-600; Cabin Door Separation; ATA 5210

A pilot encountered turbulence while in flight. The “cabin door—open” warning light was immediately followed by separation of the upper cabin door from the aircraft (P/N 250002-505). The pilot executed a safe emergency landing, then delivered the aircraft to maintenance for inspection. The microswitches controlling the door’s security warning light were found to be functioning properly. The respondent states: “The door was retrieved and the latching mechanism was found intact and operational.” No speculation as to cause was provided. (No description of how they found the door, either!)

Part Total Time: 4763.7 hours

 

ACCESSORIES

THROTTLE CONTROL CABLE

The Associate Manager, Atlanta Aircraft Certification Office, ACE-115A, submitted the following article. (The article is published as it was received.)

The FAA investigation of a recent fatal accident of a reciprocating engine powered airplane revealed an improperly maintained engine control cable. The pilot of the airplane involved in the accident stated that while in cruise flight at 2,500 feet, the engine suddenly began to “sputter”. The RPM was 700 to 800 and even though he moved the throttle in and out several times, the engine remained at 700 to 800 RPM; the throttle position made no difference. The pilot elected to make a forced landing on a highway but collided with trees and power lines. The airplane was destroyed by a post crash fire.

The subsequent investigation by the FAA and the NTSB revealed that the throttle cable had broken inside the sleeve and was not able to function. The airplane was several years old but the engine throttle cable had never been replaced. It could not be determined from the maintenance records when or if the throttle cable had been serviced, i.e. oiled.

The recommendations contained in this article are applicable to all reciprocating engine powered airplanes. Older airplanes are of a greater concern, but even new airplanes can be susceptible to similar types of failure if recommended maintenance is not performed. Proper operation and maintenance will mitigate the effects of mechanical and environmental induced wear and tear experienced during operation of the airplane and engine.

The FAA recommends that mechanics review the guidance contained in Advisory Circular (AC) 20-143 “Installation, Inspection and Maintenance of Controls for General Aviation Reciprocating Aircraft Engines” dated June 6, 2000. This AC provides guide lines for maintenance of engine control cables and linkages in general aviation airplanes. It is recommended that all maintenance technicians and inspectors become familiar with this document and use it to supplement data found in the airplane/engine maintenance manuals and service bulletins.

FOR FURTHER INFORMATION CONTACT: Jerry Robinette, Senior Propulsion Engineer, Propulsion & Services, Atlanta Aircraft Certification Office, ACO-CE118A-ATL, One Crown Center, Suite 450, 1895 Phoenix Blvd., Atlanta, GA 30349; telephone: (770) 703-6096; fax: (770) 703-6097.

 


POWERPLANTS AND PROPELLERS

CONTINENTAL

Continental; (model unknown); Broken Crankshaft; ATA 8520

Very little information accompanied this report. One engine on a Cessna 421B experienced a broken crankshaft at the number two main journal (P/N TCM 652832). The report only notes there were no signs of oil starvation or engine case fretting. The engine cases themselves were damaged beyond repair.

Part Total Time: (unknown).

 

Continental; GTSIO-520L2B; Engine Case Crack; ATA 8500

A crack was found in this engine’s case, in close proximity to a number three cylinder through-bolt, radiating downwards several inches. The mechanic writes AD 77-13-22 addresses a similar issue, but not on these model engines. “This (crack) has happened to this engine once before, two years ago.” No times on parts or causes were provided in this report.

Part Total Time: (unknown).

 

Continental; IO-240-B; Engines Shutting Down; ATA 7320

The Associate Manager, Atlanta Aircraft Certification Office, ACE-115A, submitted the following article. (The article is published as it was received.)

There have been reports of Teledyne Continental Motors (TCM) model IO-240-B engines shutting down or “running rough” when the power is reduced to idle. It should be noted that fuel flows in low horsepower engines are proportionally less than in higher horsepower engines. Therefore, less stability margin exists at low power levels/low fuel flow rates and idle fuel flow stability is more sensitive to variations in maintenance practices. For example, differences in or improperly calibrated gauges can impact fuel flow stability. In most situations, enhanced focus on maintenance practices has resolved the problems, but TCM has also introduced design improvements to address this issue, i.e. to make the engine less sensitive to low fuel flow rates and has issued service documents to address this condition.

TCM has issued Service Bulletin, SB04-4A, and Service Information Letters, SIL04-9 and SIL-05-5, to address the idle stability problem on the IO-240 engine models. In addition, Service Information Directive, SID97-3C, contains procedures and specifications for adjustment of all TCM continuous flow fuel injection systems. These service instructions and other product improvements are listed in SIL05-6, dated February 25, 2005.

The FAA recommends compliance with all TCM service/maintenance documents including those presented in TCM SIL 05-6 when performing maintenance on the IO-240-B engine. Specifically, Service Bulletin SB04-4A, SIL04-9 and SIL05-5 address the idle stability issue discussed above. In addition, SID97-3C, contains procedures and specifications for adjustment of all TCM continuous flow fuel injection systems.

The complete text of TCM SIL 05-6, SB04-4A, SIL04-9, SIL05-5 and SID97-3C and the other documents listed in SIL05-6 are available on the TCM website: http://www.tcmlink.com/ . A free printed copy can be obtained by writing to the TCM Service Department at Teledyne Continental Motors, P.O. Box 90, Mobile, AL 36601 or by calling them at (888) 826-2325.

FOR FURTHER INFORMATION CONTACT: Jerry Robinette, Senior Propulsion Engineer, Propulsion & Services, Atlanta Aircraft Certification Office, ACO-CE118A-ATL, One Crown Center, Suite 450, 1895 Phoenix Blvd., Atlanta, GA 30349; telephone: (770) 703-6096; fax: (770) 703-6097.

 


Continental; IO520; Main Bearing Failure; ATA 8520

The mechanic describes one of this engine’s main bearings as “...spun...”, whose rotation cut off the oil supply to the number two cylinder connecting rod. Friction and inertia provide the energy to send the connecting rod through the engine case. No speculation for the spun bearing was provided, but time since overhaul was given as 1,676 hours.

Part Total Time: 3,364 hours.

 

Continental; TSIO 520R; Failed Exhaust Valve; ATA 8530

It was close to noon and 17,000 feet over Pueblo, Colorado, when this pilot experienced a loud backfire, severe vibration, and a loss of engine power. The Cessna T210 was IFR to Denton, Texas. “I immediately reduced power and the vibration stopped,” writes the pilot. “I declared an emergency with Center and asked for the nearest suitable airport which had good weather. Colorado Springs, which was VFR, was offered and accepted.” He reported having sufficient power to assist in a controlled descent to the airport where a safe landing was made. Maintenance found approximately forty percent of an exhaust valve head (P/N 637781) had given away, severely damaging cylinder number one. The broken valve piece was found in the intake tube, having previously contacted both the piston and cylinder head surfaces. No speculation as to cause of the valve’s failure was provided.

Part Total Time: (unknown).

 

Continental; TSIO-520VB; Failed Connecting Rod; ATA 8520

This Cessna 402 experienced an engine failure, but the report provides no circumstances of its occurrence. The submitting mechanic speculates a capnut for connecting rod number six (P/N 643299) loosened, followed by the bolt’s head shearing off (P/N 629340).

Part Total Time: 700 hours.

 

GARRETT

Garrett; TF731-2-2B; Fuel Pump Failure; ATA 7314

As power was advanced for takeoff in this Lear 35, the left engine spooled down and then died. Maintenance said, “(The) fuel pump failed fuel discharge pressure tests during our troubleshooting per the Garrett Light Maintenance Manual.” They replaced the fuel pump with a serviceable unit and performed the required engine-performance checks including: EEC (electronic engine control) adjustments, manual mode adjustment, manual mode transfer, overspeed solenoid, and leak checks according to the (above) manual. No speculation of cause or recommendation, or time since part overhaul was provided.

Part Total Time: 11,134.7 hours.

 

HONEYWELL

Honeywell; 331-10; Cracked Oil Pump Housing; ATA 7261

While in flight, a Mitsubishi B60 had fluctuating torque and oil pressure indications. The pilot made a precautionary landing at Altoona, Pennsylvania. Subsequent engine disassembly revealed the gearbox scavenge oil pump housing (P/N 3101320-1) to be cracked. The mechanic notes: “Approximately seven hours prior (to the cracked


pump housing) the number eight stainless oil scavenge line cracked. It is believed oil pressure cycling from the line failure fractured the scavenge pump housing.” The oil pump was replaced. (Pump time since overhaul was given as approximately 4,900 hours.)

Part Total Time: (unknown).

 

LYCOMING

Lycoming; IO360-A3B6D; Failure of Cylinder Attach Studs and Bolts; ATA 8530

A pilot reported his engine was beginning to run rough. Engine monitor readings indicated the number two cylinder had failed, prompting a safe landing at Reno. The subsequent maintenance investigation found both upper through-bolts and both upper cylinder attach studs for the number two cylinder had failed at the cylinder flange. Additionally, the lower aft through-bolt for the number one cylinder was found to have failed at its flange. The writer states: “The engine had a total time of (4382.9) hours and had been overhauled 1540.9 hours previously....” All four cylinders had been replaced at 4,177.7 hours, giving 205.2 hours actual part time. “Failure of the studs and bolts appears to be consistent with either under-torque or over-torque of the nuts at installation.” (The submitter gives 4,832.9--a common transposition error, if the math is going to work.)

Part Total Time: 205.2 hours.

 

Lycoming; O-320E2D; Failed Exhaust Valve Stem; ATA 8530

A Cessna 150 lost power and made a forced, but uneventful, landing. Maintenance inspection found no compression on the number four cylinder. Further observation revealed the exhaust valve stem (P/N 75068) had failed.

Part Total Time: (unknown).

 

Lycoming; O-320; Leaking Carburetor; ATA 7322

The mechanic describes this Cessna 172 as having leaked gasoline into the engine airbox and cowling for an unspecified period of time, but perhaps as much as 400 hours. At the inevitable point of inspection and teardown of the Marvel Schebler carburetor (model 4SPA), he found the simple omission of the float shaft cotter pin (P/N A82-11) as the offending culprit. He states: “...the log book records this carburetor to have been overhauled by Precision Airmotive and purchased from Aircraft Spruce & Specialty in June, 2004.”

Part Total Time: 400 hours.

 

PRATT AND WHITNEY

Pratt and Whitney; JT8D-17; Engine Compressor Failures; ATA 7230

(The following article’s text is printed as received from Transport Canada.)

“Shortly after departure and climbing through 3,300 feet AGL, the crew of a commercial air carrier reported a loud bang that sounded much like an engine compressor stall. Cockpit indications-revealed rapidly declining N1 (low-pressure compressor) and N2 (high-pressure compressor) readings on the number 1 engine gauges. The exhaust gas temperature (EGT) had exceeded the highest temperature on the gauge, and the cockpit crew immediately shut down the faulty engine. The crew declared an emergency, landed uneventfully, then taxied back to the departure gate.

“Investigation carried out by the Transportation Safety Board of Canada (TSB) revealed that all engine indications were normal at start-up, taxi, take-off, and climb phases until the sudden loud bang occurred.


Company maintenance personnel found evidence of extremely high temperatures in the turbine sections. Turbine nozzle guide vanes were intact but revealed heat distress on the trailing edge. The high-pressure turbine (HPT) blades had melted from about 30 degrees of the span and outboard. All three stages of the low-pressure turbine (LPT) had melted at various lengths, and solidified pools of metal had formed on the inside of the exhaust nozzle outlet. Noticeable damage to the 3rd stage compressor disk was also discovered, however, there was no evidence of foreign object ingestion.

“Prior to departure on the previous day, a review of company maintenance documents revealed that the #1 engine compressor surging had occurred during start-up and acceleration from idle. During taxi back to the ramp for maintenance attention, at least five more surging events occurred. Maintenance personnel then followed the engine manual instructions and replaced the pressure ratio bleed control valve and the start bleed control valve. Inspection of the compressor section was not carried out, nor was it required according to the engine maintenance trouble-shooting instructions. A subsequent low power engine run-up led maintenance personnel to believe that the 'compressor surging' problem was solved. The aircraft then returned to service and operated for three hours before the subject in-flight failure occurred. Prior to flight on the day of the failure, engine performance data was reviewed and it was noted that EGT had increased by 20°C and N2 had increased by 2.5%. This type of deterioration in engine performance parameters is a dependable indicator of progressive gas-flow inefficiencies, compressor turbine damage, and incipient engine failure. TSB engineering analysis of the damaged engine components revealed that the majority of the compressor blade roots exhibited fatigue fractures consistent with reverse bending. Reverse bending of the compressor blades is a reliable indication of compressor 'stall'. Compressor stalls can cause reverse bending of the compressor blades, causing fatigue fractures, resulting in engine failures such as seen in this particular event.

“Although not required by the engine manufacturer’s troubleshooting guidelines, it is most likely that a maintenance high-powered engine ground run-up and engine performance analysis, followed by a compressor borescope inspection, would have discovered the previously damaged blades. Transport Canada Civil Aviation (TCCA) strongly advises maintainers, operators and other responsible persons that compressor surging should be given the same attention as compressor stalls. Surges should be considered minor stalls and should not be underestimated in the damage that can occur. It is evident that compressor surges and stalls can induce latent fatigue fractures culminating in engine failures.

“In the absence of the manufacturer’s maintenance instructions directed specifically towards monitoring the effects of compressor surges, operators are advised to apply these instructions provided for monitoring the effects of compressor stalls. Any defects or further occurrences should be reported by sending a Service Difficulty Report to Transport Canada, Continuing Airworthiness, Ottawa.”

For further information, contact a Transport Canada Centre, or Mr. Barry Caldwell, Continuing Airworthiness, Ottawa: telephone (613) 952-4358, facsimile (613) 996-9178, or e-mail caldweb@tc.gc.ca. (The website given for this document is  www.tc.gc.ca/CivilAviation/certification/menu.htm)

Part Total Time: (unknown)

 

ROLLS-ROYCE

Rolls-Royce; 250-C20; Grinding Noise; ATA 7200

The pilot of this Bell 206B helicopter “...reported hearing a grinding noise from the engine, followed by a chip detection light...” This event triggered a power-on precautionary landing. The aircraft was returned to service with another engine while its original was sent to Essential Turbines, Inc., of Canada for further evaluation. No speculation was offered with this report. The following time summations were provided: aircraft total time as 16,572.2; engine total time as 9,341.0; engine cycles since new as 5,393; engine gearbox time since new as


9,341.0 and since overhaul as 9,341.0; engine compressor time since new as 9295.8 and since overhaul as 2914.8; compressor cycles since new as 20475 and since overhaul as 4355; engine turbine time since new 11466.5 and since overhaul as 1655.9; engine cycles since new as 22971 and since overhaul as 3707...hours.

Part Total Time: (unknown).

 

TURBOMECA

Turbomeca; Arruis 1A; Failed Exhaust Studs; ATA 7810

The respondent writes, “Three out of four struts that hold the outside part of the exhaust--failed (P/N 0319778440). Total time of the part is unknown. Turbomeca thinks the problem is related to a high vibration in the starter-generator. The vibration level was (measured at) .04, well below the limit.” (This engine is mounted on the Aerospatiale 355N).

Part Total Time: (unknown).

 

AIR NOTES

ELECTRONIC VERSION OF FAA FORM 8010-4, MALFUNCTION OR DEFECT REPORT

One of the recent improvements to the Flight Standards Service Aviation Information Internet web site is the inclusion of FAA Form 8010-4, Malfunction or Defect Report. This web site is still under construction and further changes will be made; however, the site is now active, usable, and contains a great deal of information.

Various electronic versions of this form have been used in the past; however, this new electronic version is more user friendly and replaces all other versions. You can complete the form online and submit the information electronically. The form is used for all aircraft except certificated air carriers who are provided a different electronic form. The Internet address is: http://av‑info.faa.gov/SDRX

When the page opens, select “M or D Submission Form” and, when complete, use the “Add Service Difficulty Report” button at the top left to send the form. Many of you have inquired about this service. It is now available, and we encourage everyone to use this format when submitting aviation, service-related information.

 

PAPER COPY OF FAA FORM 8010-4, MALFUNCTION OR DEFECT REPORT

In the past, the last two pages of the Alerts contained a paper copy of FAA Form 8010-4, Malfunction or Defect Report. To meet the requirements of *Section 508, this form will no longer be published in the Alerts; however, the form is available on the Internet at: http://forms.faa.gov/forms/faa8010‑4.pdf . You can still download and complete the form as you have in the past.

*Section 508 was enacted to eliminate barriers in information technology, to make available new opportunities for people with disabilities, and to encourage development of technologies that will help achieve these goals.

 


INTERNET SERVICE DIFFICULTY REPORTING (iSDR) WEB SITE

The Federal Aviation Administration (FAA) Internet Service Difficulty Reporting (iSDR) web site is the front-end for the Service Difficulty Reporting System (SDRS) database that is maintained by the Aviation Data Systems Branch, AFS-620, in Oklahoma City, Oklahoma. The iSDR web site supports the Flight Standards Service (AFS), Service Difficulty Program by providing the aviation community with a voluntary and electronic means to conveniently submit in-service reports of failures, malfunctions, or defects on aeronautical products. The objective of the Service Difficulty Program is to achieve prompt correction of conditions adversely affecting continued airworthiness of aeronautical products. To accomplish this, Mechanical Reliability Reports (MRRs), Malfunction or Defect Reports (M or Ds), or Service Difficulty Reports (SDRs) as they are commonly called, are collected, converted into a common SDR format, stored, and made available to the appropriate segments of the FAA, the aviation community, and the general public for review and analysis. SDR data is accessible through the “Query SDR data” feature on the iSDR web site at: http://av‑info.faa.gov/SDRX .

A report should be filed whenever a system, component, or part of an aircraft, powerplant, propeller, or appliance fails to function in a normal or usual manner. In addition, if a system, component, or part of an aircraft, powerplant, propeller, or appliance has a flaw or imperfection, which impairs or may impair its future function, it is considered defective and should be reported under the Service Difficulty Program.

The collection, collation, analysis of data, and the rapid dissemination of mechanical discrepancies, alerts, and trend information to the appropriate segments of the FAA and the aviation community provides an effective and economical method of ensuring future aviation safety.

The FAA analyzes SDR data for safety implications and reviews the data to identify possible trends that may not be apparent regionally or to individual operators. As a result, the FAA may disseminate safety information to a particular section of the aviation community. The FAA also may adopt new regulations or issue airworthiness directives (ADs) to address a specific problem.

The iSDR web site provides an electronic means for the general aviation community to voluntarily submit reports, and may serve as an alternative means for operators and air agencies to comply with the reporting requirements of 14 Title of the Code of Federal Regulations (CFR) Section 121.703, 125.409, 135.415, and 145.221, if accepted by their certificate-holding district office. FAA Aviation Safety Inspectors may also report service difficulty information when they conduct routine aircraft maintenance surveillance as well as accident and incident investigations.

The SDRS database contains records dating back to 1974. At the current time, we are receiving approximately 40,000 records per year. Reports may be submitted to the iSDR web site on active data entry form or submitted hardcopy to the address below.

The SDRS and iSDR web site point of contact is:

John Jackson
Service Difficulty Reporting System, Program Manager
Aviation Data Systems Branch, AFS-620
P.O. Box 25082
Oklahoma City, OK 73125
Telephone: (405) 954-6486
SDRS Program Manager e-mail address: 9‑AMC‑SDR‑ProgMgr@faa.gov

 


IF YOU WANT TO CONTACT US

We welcome your comments, suggestions, and questions. You may use any of the following means of communication to submit reports concerning aviation-related occurrences.

Editor:  Daniel Roller (405) 954-3646
FAX:    (405) 954-4570 or (405) 954-4655

E-mail address:   Daniel.Roller@faa.gov

Mailing address: FAA, ATTN: AFS-620 ALERTS, P.O. Box 25082 , Oklahoma City, OK 73125-5029

You can access current and back issues of this publication from the internet at:
http://av‑info.faa.gov/ . Select the General Aviation Airworthiness Alerts heading.

 

AVIATION SERVICE DIFFICULTY REPORTS

The following are abbreviated reports submitted for the previous month, which have been entered into the FAA Service Difficulty Reporting (SDR) System database. This is not an all inclusive listing of Service Difficulty Reports. For more information, contact the FAA, Regulatory Support Division, Aviation Data Systems Branch, AFS-620, located in Oklahoma City, Oklahoma. The mailing address is:

FAA
Aviation Data Systems Branch, AFS-620
PO Box 25082
Oklahoma City, OK 73125

To retrieve the complete report, click on the Control Number located in each report. These reports contain raw data that has not been edited. Also, because these reports contain raw data, the pages containing the raw data are not numbered.

If you require further detail please contact AFS-620 at the address above.


Federal Aviation Administration

Service Difficulty Report Data

 

Sorted by aircraft make and model then engine make and model. This report derives from unverified information submitted by the aviation community without FAA review for accuracy.

Control Number

Aircraft Make

Engine Make

Component Make

Part Name

Part Condition

Difficulty Date

Aircraft Model

Engine Model

Component Model

Part Number

Part Location

2005FA0000035

 

 

 

LIFE VEST

FAILED

12/16/2004

 

 

 

GA12P0201

CABIN

INDIVIDUAL FLOAT DEVICE FAILED CELL PRESSURE TEST DUE TO INFLATION VALVE RUPTURE. DOM: NOV 1981.

CA040629002

 

ALLSN

 

BEARING

FAILED

6/29/2004

 

AE3007C

 

 

NR 4 

(CAN) DURING CRUISE AT 43,000 FT, CREW RECEIVED CHIP DETECTOR MESSAGE, FOLLOWED BY AN OIL FILTER BYPASS MESSAGE ON THE RT ENGINE. A/C WAS BEING FLOWN FOR MAINTENANCE VISIT TO THE MFG SERVICE CENTER. CREW ELECTED TO CONTINUE F LIGHT AFTER RECEIVING THE ABOVE MESSAGES. 15 MINUTES AFTER RECEIVING THE OIL FILTER BYPASS MESSAGE, OIL PRESSURE BEGAN TO DROP AND THE CREW ELECTED TO SHUTDOWN THE ENGINE. CREW ELECTED TO CONTINUE SINGLE ENGINE FLIGHT TO DESTINATION. INITIAL INVESTIGATION INDICATES A NR 4 BEARING FAILURE. ENGINE SENT TO FOR REPAIR, FURTHER DETAIL WILL BE SUBMITTED UPON DISASSEMBLY OF ENGINE.

C7GR861J

 

LYC  

HONEYWELL

MANIFOLD

MISINSTALLED

8/20/2004

 

LTS101750B1

 

419110003

PT MODULE

LTS101-750B-1 ENGINE, SN: LE-48166BEF WAS RECEIVED BY THIS REPAIR STATION (CRS NR C7GR861J) FOR ROUTINE MAINTENANCE. SINCE WE HAD RECEIVED SOME NEW MANIFOLD ASSEMBLIES WITH IMPROPERLY TORQUED BOLTS (16 EA) THAT SECURE EIGHT COVERS ON THE INJECTOR BLOCKS, DECIDED TO PERFORM A TORQUE CHECK ON THIS FUEL MANIFOLD (TSN = 900 HRS). BREAKAWAY TORQUES AS LOW AS 18 IN/LB WAS OBSERVED. THE PROPER TORQUE IS 40-45 IN/LB. THIS CONDITION HAS BEEN REPORTED TO HONEYWELL, PHOENIX FOR PROPER INVESTIGATION AND RESOLUTION.

CA040415006

 

PWA  

 

ENGINE

DAMAGED

4/2/2004

 

PT6A28

 

 

 

ENG REMOVED AFTER A/C DRIFTED TO LT SIDE OF RWY & HIT A 4 FT SNOWBANK. NLG COLLAPSED & ENG HIT BANK AT MAX PWR. EXHAUST DUCT & GG CASE HAD OUTER SKIN BUCKLING. 2ND STAGE REDUCTION PLANET GEAR CARRIER BENT, PT RUB DAMAGE ON BLADE TIPS. COMP BLADES, STATORS & IMPELLER RUB DAMAGE. PT DISK DISPLACED, COMPRESSOR RUB DAMAGE GG CASE. RGB OIL PRESS XFER TUBE BENT & CONNECTING ELBOW BROKEN. IN TEST CELL, DURING TEST FOUND ENG PERFORMANCE ACCEPTABLE, BUT A LOUD RUB NOISE HEARD ON RUNDOWN, TRACED TO WORN SPLINES ON RGB HOUSING. CHANGED HOUSING. REMOVED FROM CELL TO INVEST 2ND STAGE GEARING, FOUND REAR FACE OF 2ND STAGE CARRIER DISTORTED. CARRIER CHANGED, ENG TESTED. NO ADVERSE NOISES ON SHUTDOWN, ENG DECLARED SERVICEABLE.

TXER096384

AEROSP

 

 

SERVO

BINDING

7/13/2004

AS355*

 

 

SC5072

TAIL ROTOR

TAIL ROTOR SERVO IS BINDING.

I05R098769

AEROSP

 

 

PRESSURE SWITCH

FAILED

8/25/2004

AS355*

 

 

MA12401

HYD SYSTEM

PRESSURE SWITCH FAILED IN 3 HRS OF OPERATION. REPLACED PART.

CA040811008

AEROSP

ALLSN

 

BLOWER

DAMAGED

8/5/2004

AS355F1

250C20F

 

355A340109

OIL COOLER

(CAN) DURING OPERATION A NOISE WAS HEARD FROM THE BACK OF THE AIRCRAFT, AIRCRAFT WAS LANDED AND DURING INSPECTION TO DETERMINE THE ORIGIN OF THE SOUND IT WAS NOTED THAT THE OIL COOLER BLOWER ASSY WAS DAMAGED AND HAD SEVERAL PIECES MISSING. THE AIRCRAFT WAS RETURNED TO BASE BY ROAD AND WAS DISASSEMBLED TO THE EXTENT REQUIRED TO INSPECT FOR OTHER DAMAGE. ONCE THE BLOWER WAS REMOVED IT WAS NOTED THAT THE FIRST STAGE OF THE ASSY HAD 2 SMALL NICKS ON 2 OF THE ROTATING BLADES. THE FIRST STAGE STATOR CASE, THE SECOND STAGE ROTATING AND STATIONARY COMPONENTS HAD EXTENSIVE DAMAGE AND WERE FOUND IN SEVERAL PIECES. SUSPECT DAMAGE COULD HAVE BEEN CAUSED BY FOD.

CA050117011

AEROSP

PWA  

 

TURBINE BLADES

DAMAGED

1/13/2005

ATR42*

PW120

 

 

ENGINE

(CAN) DURING CRUISE THE PILOT REPORTED A (PUFF) FROM THE ENGINE ACCOMPANIED BY A LOSS OF TORQUE. POWER LEVER ADVANCEMENT RESULTED IN ENGINE TEMPERATURE INCREASE AND AN OIL SMELL AND SMOKE IN THE CABIN. THE ENGINE WAS SHUT DOWN, AN EMERGENCY DECLARED AND THE FLIGHT DIVERTED. SUBSEQUENT INSPECTION REVEALED DAMAGED TURBINE BLADES. MFG WILL INVESTIGATE THE INCIDENT AND SUPPLEMENT THIS REPORT TO PROVIDE ROOT CAUSE, ONCE ESTABLISHED.

CA040810003

AEROSP

PWA  

 

O-RING

FAILED

8/7/2004

ATR42300

PW120

 

 

HYD SYSTEM

(CAN) ENROUTE, (GREEN SYS) LOW LEVEL PRESS INDICATION OBSERVED. THE CREW ACCOMPLISHED THE CHECK LIST AND CONTINUED TO YZF. THE AIRCRAFT LANDED WITHOUT INCIDENT AND WAS TOWED FROM THE RUNWAY. THE O-RING AND BACK-UP RING AT THE ACCUMULATOR FITTING WERE REPLACED, THE AIRCRAFT WAS LEAK CHECKED AND RETURNED TO SERVICE.

CA050119008

AEROSP

PWA  

 

PROBE

STICKING

1/3/2005

ATR42300

PW120

 

 

ANGLE OF ATTACH

(CAN) AFTER DEPARTING, THE CREW OBSERVED A STICK SPURRIOUS SHAKER WARNING. THE AIRCRAFT RETURNED TO POINT OF DEPARTURE. THE ANGLE OF ATTACK PROBE WAS FOUND TO BE STICKING, MAINTENANCE LURICATED THE PROBE AND THE SYSTEM WAS CHECKED SERVICEABLE. THE AIRCRAFT WAS RETURNED TO SERVICE.

CA041124011

AEROSP

PWA  

 

DRIVE ASSY

FRACTURED

11/10/2004

ATR72

PW124B

 

 

GEARBOX

(CAN) DURING CRUISE, ENGINE OIL PRESSURE DROPPED TO ZERO FOLLOWED BY AN UNCOMMANDED ENGINE SHUTDOWN. A SINGLE ENGINE LANDING WAS CARRIED OUT AT DESTINATION. SUBSEQUENT INVESTIGATION HAS EVIDENCED A FRACTURED (ACCESSORY GEARBOX DRIVE) TOWERSHAFT. PWA WILL INVESTIGATE THE EVENT AND REVISE THIS REPORT TO REFLECT ROOT CAUSE, ONCE DETERMINED.

CA041122014

AEROSP

PWA  

 

ENGINE

FAILED

10/26/2004

ATR72

PW124B

 

 

LEFT 

(CAN) DURING CRUISE, PROPELLER SPEED DECREASED ACCOMPANIED BY MASTER WARNING AND CCAS+LOW ALERTS. THE CREW SECURED THE ENGINE, DECLARED PAN PAN AND COMPLETED A SING LT ENGINE LANDING AT DESTINATION. MFG WILL MONITOR THE INVESTIGATION AND AMEND THIS REPORT TO REFLECT ROOT CAUSE ONCE DETERMINED.

TL9R200500002

AIRBUS

 

 

BRAKE

MAKING METAL

1/20/2005

A300*

 

 

C200601004

MLG 

OUR REPAIR SHOP REPORTS THAT THE ROTORS IN THIS BRAKE PN HAVE A HISTORY OF FALLING APART. WHEN THIS HAPPENS, DAMAGE TO THE TORQUE TUBE CAN OCCUR WHICH WILL SEVERELY DEGRADE THE PERFORMANCE OF THE BRAKE.

TL9R200500001

AIRBUS

 

 

BRAKE

MAKING METAL

1/20/2005

A300*

 

 

C200601004

MLG 

OUR REPAIR SHOP REPORTS THAT THE ROTORS IN THIS BRAKE PN HAVE A HISTORY OF FALLING APART. WHEN THIS HAPPENS, DAMAGE TO THE TORQUE TUBE CAN OCCUR WHICH WILL SEVERELY DEGRADE THE PERFORMANCE OF THE BRAKE.

CA040630005

AIRBUS

GE  

 

FITTING

LOOSE

6/29/2004

A310304

CF680C2*

 

A5784365500400

PRESSURE LINE

(CAN) ON FINAL APPROACH, WHEN FLAP/SLAT WERE EXTENDED, THE HYDRAULIC RESERVOIR LOW LEVEL ECAM WARNING CAME ON. AIRCRAFT OVERSHOT AND CHECKLIST PROCEDURE INDICATE A FAILURE OF GREEN HYDRAULIC SYSTEM. ALTERNATE GEAR EXTENSION PERFORMED. DURING INVESTIGATION, FOUND THE GREEN SYSTEM PRESSURE LINE FITTING LOOSE ON THE RT KRUGER FLAP ACTUATOR. LINE TIGHTENED AND SYSTEM WAS VERIFIED SERVICEABLE IAW THE MM.

CA041202002

AIRBUS

CFMINT

 

SELECTOR VALVE

FAILED

12/2/2004

A319114

CFM565A1

 

114079016

MLG 

(CAN) FAULT: AFTER T/O AND GEAR UP, NR 1 LGCIU ECAM MSG ON. ALSO DURING A GO-AROUND AFTER GEAR SELECTED UP, MASTER (RED) WARNING CAME ON WITH MSG. (GEAR DISAGREEMENT) DURING APROX. 10 SEC.ACTION: MLG DOOR SEL VALVE REPLACED IAW MM 32-31-34. FUNCTIONAL CHECK CARRIED OUT OK, LEAK CHECK C/OUT SERVICE.

CA041203002

AIRBUS

GE  

 

CONTROL VALVE

INOPERATIVE

12/3/2004

A319114

CFM565A

 

C24736001

NLG STEERING

(CAN) IN CRUISE, WHEEL NOSE WHEEL STEERING FAULT . TRIED RESET ANTI-SKID /NW STEERING SWNO FIX. NO NW STEERING ON LANDING. TOWED TO GATE. TESTED BSCU 1 AND 2 FAULTED NLG STEERING SERVO FTN 6GC. IAW TSM AND AMM REPLACED NLG STEERING SERVO FTN 6GC. OPERATION TEST PERFORMED BSCU 1 AND 2 TESTED, NO FAULTS.

CA040615001

AIRBUS

CFMINT

 

CONTROL UNIT

FAILED

6/15/2004

A320211

CFM565A1

 

 

TE FLAPS

(CAN) FAULT: ON FINAL APPROACH, WHEN FLAP 1 SELECTED, ONLY SLATS CAME OUT. NO FLAPS, RECYCLED TWICE NOJOY. SLATS ONLY LANDING CARRIED OUT. ACFT OUT OF SERVICE FOR INVESTIGATION. COMMENTS: FURTHER INFO WILL FOLLOW.

CA050111002

AIRBUS

CFMINT

 

SERVO

INTERMITTENT

1/11/2005

A320211

CFM565A1

 

 

SPOILER

(CAN) FAULT: JUST PRIOR TAKE-OFF, FLIGHT RECEIVED A FLT CTL SPOILER 1 FAULT. CREW TAXIED ONTO A TAXIWAY AND PERFORMED A SUCCESSFUL RESET. HOWEVER, AT 3000 FT/210 KNOTS ON CLIMB, THE FAULT RETURNED AGAIN. FURTHER INTO THE FLIGHT IN CRUISE SLAT SYSTEM. ACTION: ACFT OUT OF SERVICE FOR INVESTIGATION.

CA040412006

AIRBUS

CFMINT

 

ENGINE

BIRD INGESTION

4/12/2004

A320211

CFM565A1

 

 

NR 1 

(CAN) FAULT: HIT 2 GEESE ON T/O HIGH SPEED REJECTED RETURNED TO GATE. FOUND EVIDENCE OF BIRD INGESTION AT NR 1 ENG. SEVERAL DAMAGED BLADES, A/C ROUTED TO HANGAR FOR ENGINE BOROSCOPE.

CA040812004

AIRBUS

CFMINT

BFGOODRICH

BOLT

BROKEN

6/20/2004

A320214

CFM565B4

31530

431304

MLG WHEEL

(CAN) ON WALK AROUND PILOT FOUND 2 TIE BOLTS (P/N 43-1304) BROKEN ON THE NR 1 MAINWHEEL ASSY, TOTAL CYCLES ON MAIN WHEEL ASSY SINCE LAST RE-FURB 427, TOTAL TIME ON TIE BOLTS UNKN.

CA041102001

AIRBUS

RROYCE

 

BOLT

SHEARED

11/2/2004

A330*

RB211TRENT77

 

NAS6605D136

RT MLG

(CAN) MSN 419 WAS UNDERGOING A C2 CHECK IN YUL. IN PREP FOR DOING A SEAL CHANGE ON RT MLG MAINT DISCOVERED SM9 PIN MIGRATED APPROX. 1INCH OUT IN THE IB DIRECTION. GEAR WAS SPLIT,AND IT WAS DISCOVERED THAT THE SM9 PIN RETENTION BOLT (NAS6605D136) HAD SHEARED AT THE HEAD. THE BOLT RETAINS THE PIN END CAPS. CAMPAIGN NR 9-0066 WAS LAUNCHED ON NOV 1 2004 TO INSPECT ALL ACFT IN FLEET A330/A340.

2004FA0000908

AMD  

GARRTT

 

HOSE

COLLAPSED

10/14/2004

FALCON10

TFE73121C

 

FAL1005D

ANTI-ICE SYS

DURING ENGINE RUN-UP, PHYSICALLY CHECKED LEADING EDGE FOR HEAT AND FOUND COLD. RT IB ANTI-ICE FLEXHOSE WAS REMOVED AND VISUALLY INSPECTED. FOUND THE INNER LINING HAD COLLAPSED, BLOCKING AIRFLOW THROUGH HOSE. HOSE WAS REPLACED WITH NEW. FAULTY HOSE WAS MARKED "3Q01". THIS FLEXHOSE, P/N FAL1005D, IS REFERENCED IN DASSAULT SERVICE BULLETIN F10-A246. THIS HOSE WAS LAST REPLACED ON 4/22/2003 AT 6213.2 HRS TTAF AND 5458 TOTAL LANDINGS BY CRS# BONR551C.

2005FA0000072

AMD  

GARRTT

 

AUDIO CONTROL

INOPERATIVE

7/15/2004

FALCON50MYST

TFE73140

 

9903333142

COCKPIT

FLIGHT CREW REPORTED ACRID SMELL IN THE COCKPIT ON APPROACH TO LANDING. NR 2 VHF COMM NOT FUNCTION REPORTED BY FLIGHTCREW. INSPECTION DID CONFIRM NR 2 COMM TRANSCEIVER WAS INOPERATIVE. REMOVED AND REPLACED WITH SERVICEABLE UNIT. ADDITIONAL TROUBLESHOOTING AND INSPECTION TO AIRFRAME AND AVIONICS RELATED COMPONENTS DID REVEAL THE AUDIO CONTROL PANEL (PN990-3333-142) NR 2 VHF COMM TRANSCEIVER. AUDIO CONTROL PANEL RETURNED FOR INSPECTION, REPAIR AND RETURNED TO SERVICE. (NM01200501124) (K)

2004FA0000888

AMRGEN

LYC  

 

CABLE

WORN

7/13/2004

AG5B

O360*

 

A9200410

THROTTLE

SWEDGED-IN PORTION OF THE CABLE GUIDE DISPLAYED .110 INCH FORE AND AFT PLAY INDICATING IMPENDING FAILURE OF THE SWIVEL JOINT. CABLE WAS REMOVED AND GIVEN FOR EVALUATION. THIS CONDITION WAS APPARENTLY CAUSED BY DIRT CONTAMINATION. (THE PROTECTIVE RUBBER BOOT OVER THE SWIVEL JOINT HAD CRACKED, ALLOWING DIRT CONTAMINATION OF THE JOINT.) THIS SUBMITTER RECOMMENDS THAT THE THROTTLE CABLE SWIVEL JOINT AND ITS RUBBER BOOT BE CLOSELY INSPECTED AT EACH 100 HOUR AND/OR ANNUAL INSPECTION TO PREVENT EXCESSIVE WARE AND SUBSEQUENT FAILURE OF THE THROTTLE CABLE. (EA07NEL200405197)

2004FA0000600

AMTR

 

 

FORK

BROKEN

6/14/2004

AEROSTARBIRD

 

 

 

NLG 

THE PILOT REPORTED THAT WHILE TAXING AFTER A LANDING, THE NOSE GEAR GAVE WAY AND THE AIRCRAFT CAME TO REST ON THE PROPELLER SPINNER. THIS IS AN AMATEUR BUILT AIRCRAFT. THE AIRCRAFT BUILDER MADE THE NOSE WHEEL FORK THAT BROKE. THEREBY LOSING THE NOSE WHEEL AND CAUSING THE NOSE GEAR LEG TO FOLD BACK AND PUTTING THE PROPELLER SPINNER ON THE PAVEMENT. SINCE THIS PART IS INSTALLED ON AN EXPERIMENTAL AIRCRAFT THERE ARE NO STANDARDS FOR THE AIRCRAFT OR ANY OF THE PARTS. PREVENTION/SOLUTION, THE PRESENT OWNER HAS RELATED THE OLD PART WAS MADE UP OF ONE QUARTER INCH 2024 T3 ALUMINUM AND THE NEW PART WILL BE ONE EIGHTH INCH 4130 STEEL, BENT TO SHAPE AND THEN HARDENED TO A HARDNESS OF 135-145.

2005FA0000029

AMTR

LYC  

 

ROD  

BENT

1/7/2005

COZY

O320*

 

 

RT BRAKE CYL ACT

RT BRAKE CYLINDER ACTUATING ROD, LOCATED BEHIND RT RUDDER PEDAL, WAS SLIGHTLY BENT AFT. THIS CONDITION CAUSED INSUFFICIENT BRAKE CYLINDER PISTON TRAVEL AND MAKING THE RT BRAKE INOPERATIVE.

2004FA0000401

AMTR

 

 

PAD  

BINDING

5/13/2004

VM1  

 

 

DP600

BRAKES

PILOT WAS IN PROCESS OF TAKEOFF ROLL, PILOT REPORTED A/C VEERED TO LT HITTING A RUNWAY LIGHT, WENT OVER SOME TERRAIN AND ENDED PARTIALLY SUBMERGED IN A BODY OF WATER. AN EXAMINATION OF THE A/C WAS CONDUCTED. THE A/C CONFIG INCLUDES A FREE CASTORING NOSE WHEEL AND BRAKES ARE OF A MOTO-GUZZI MOTORCYCLE. LT BRAKE FOUND TO BE DRAGGING SUBSTANTIALLY, AFFECTING THE SMOOTH ROTATION OF THE LT MAIN GEAR WHEEL. THE RT WHEEL AND BRAKE WERE SATISFACTORY. THE BRAKE WAS REMOVED. IT WAS FOUND THE DESIGN OF WIRE LOOP USED AS A MEANS TO HOLD BRAKE PADS ALIGNED, APPLIES CONSTANT RESISTANCE ON THE BRAKE PADS. THIS CONSTANT RESISTANCE PREVENTS THE BRAKE PADS FROM FLOATING AT ALL, THERE IS MINIMAL CLEARANCE, FROM THE BRAKE DISC.

2004FA0000878

AMTR

ROTAX

 

AXLE

SEPARATED

10/8/2004

ZENITHCH701

ROTAX912UL

 

 

WHEEL ASSEMBLY

LEFT MAIN AXLE SEPARATED FROM BACKING PLATE AT LANDING CAUSING MAIN SPRING TO DIG IN, WHICH CAUSED THE PLANE TO NOSE OVER. INSPECTION OF THE AXLE ASSEMBLY REVEALED VERY LITTLE WELD PENETRATION AND THE WHOLE DESIGN WAS VERY INADEQUATE FOR THE TYPE OF OPERATIONS THAT THIS GEAR ASSEMBLY MARKETED TO.

2004FA0000931

AMTR

ROTAX

 

STRUT

BROKEN

12/16/2004

ZODIAC

ROTAX912S2

 

 

LT MLG

THE LT MAIN GEAR STRUT FAILED AT THE LOWER WELDMENT WHERE THE STRUT ATTACHES TO THE FORK. THIS DAMAGE HAD PROGRESSED AROUND THE ATTACHMENT IN THE FORM OF A CRACK UNTIL WEEKEND TO THE POINT OF FAILURE. THIS PART HAD BEEN FABRICATED BY THE KIT MANUFACTURER.

CA040610014

BAC  

LYC  

 

SPRING

FAILED

6/7/2004

146200A

ALF502R5

 

HC323L0001000

NLG 

(CAN) UPON DEPARTURE, THE CREW REPORTED LOUD CLUNK NOISE UNDER FLIGHT DECK DURING GEAR RETRACTION. MAINTENANCE INSPECTED AIRCRAFT AND FOUND LT NLG ASSIST SPRING ASSEMBLY HAD FAILED AND CAUSED A 12 X 8 HOLE IN UPPER NOSE WELL. ASSISTOR SPRING WAS REPLACED AND HOLE WAS REPAIRED IAW THE PRINCIPALS OF RIL HC537H9252 AT ISSUE 1 IN REFERENCE TO BARA/AVR/6774/04-DC. GEAR SWINGS WERE CARRIED OUT AS SERVICEABLE AND AIRCRAFT WAS RETURNED TO SERVICE. TIMES FOR THIS PART ARE LISTED AS AIRCRAFT TIMES.

CA040505001

BAC  

LYC  

 

WHEEL

CRACKED

5/1/2004

146200A

ALF502R5

 

AHA1481

MLG 

A/C IN HEAVY MX IN YHZ AND HAD JUST BEEN TAKEN OFF THE JACKS WHEN ENGINEERS NOTED THAT NR 3 MAIN WHEEL WAS FLAT. THE WHEEL WAS REPLACED ALONG WITH ITS MATE AS PER COMPANY POLICY, THE WHEEL WAS ROUTED TO WHEEL/BRAKE SHOP AND WENT THROUGH A BUILD (22) INSPECTION. NDT FOUND THE INNER WHEEL HALF HAD CRACK EMANATING FROM ONE OF THE THREE-FUSE PLUGHOLE.THE INNER WHEEL HALF P/N AHA1481 IS FOUND IN THE DUNLOP CMM IPL 32-42-59 FIG 1 ITEM 280.THIS WHEEL WAS ON BUILD 21 AND HAD BEEN NDT AT THAT TIME WITH NO DEFECTS NOTED AT THE TIME. THIS MATTER HAS BEEN BROUGHT TO THE ATTN OF THE MANUF AND WE HAVE ASKED WHAT HAS BEEN THE OCCURRENCE ON THIS TYPE OF FAILURE AND HAVE ASKED WHETHER OR NOT THEY WOULD LIKE TO SEE THE COMPONENT FOR ANALYSIS. WILL FOLLOW-UP ON THE INCIDENT ONCE WE HEAR BACK FROM THE MANUF WITH THEIR RECOMMENDATIONS.

2005FA0000014

BBAVIA

CONT

 

SPAR

CRACKED

1/21/2005

7AC  

A65*

 

 

WING 

DURING PRE-PURCHASE, COMPLIED WITH INSPECTION. BOTH SPARS IN BOTH WINGS WERE FOUND TO HAVE LOOSE AND MISSING NAILS THAT HOLD RIBS OT THE SPARS. SEVERAL LONGITUDINAL CRACKS WERE FOUND. RECOMMENDATION TO OWNER WAS TO REPLACE ALL WOOD SPARS, WITH STC METAL SPARS.

2005FA0000038

BBAVIA

LYC  

 

BOLT

IMPROPER PART

11/2/2004

7KCAB

IO320*

 

NAS 

MLG ATTACH

DURING ANNUAL INSPECTION, IT WAS FOUND THAT ONE OF THE NAS BOLTS HOLDING THE IB END OF THE LANDING GEAR WAS TOO SHORT AND DID NOT GO ALL THE WAY THROUGH THE NAS NUT. THESE BOLTS WERE INSTALLED AT THE FACTORY, DURING A REPAIR IN 2001. FAILURE WOULD RESULT IN ONE LANDING GEAR LEG COLLAPSING. (EA17200504802)

CA040504004

BEECH

PWA  

 

SUPPORT BRACKET

CRACKED

4/29/2004

100BEECH

PT6A28

 

11552405813

ELEV BELLCRANK

(CAN) DURING AIRCRAFT INSPECTION, IT WAS NOTED THE AFT RT ELEVATOR BELLCRANK SUPPORT BRACKET P/N 115-524058-13 WAS CRACKED. THE CRACK EXTENDED APPROX. 1.5 INCHES VERTICALLY AROUND THE BELLCRANK PIVOT BOLT ATTACHMENT.

CA040810004

BEECH

PWA  

 

LINE

WORN

8/6/2004

1900C

PT6A65B

 

11492000023

ENGINE FUEL

(CAN) WHEN INSTALLING INSPECTION PANEL ON LT OB NACELLE FOUND FUEL LINE FROM FUEL BOWL FORWARD TO ENGINE WAS CHAFING ON BULKHEAD IN SIDE OF NACELLE. THE LINE WAS WORN ABOUT A QUARTER OF ITS WALL THICKNESS.

CA041004003

BEECH

PWA  

 

DISC

FRACTURED

9/26/2004

1900C

PT6A65B

 

114800817

BRAKES

(CAN) ON PUSH BACK INTO THE HANGAR AN UNUSUAL NOISE WAS HEARD FROM NR 2 MAINWHEEL. ON REMOVING THE MAIN WHEEL, A SECTION OF THE STATIONARY DISC FELL OUT OF THE BRAKE ASSEMBLY. WHEN THE BRAKE ASSY WAS REMOVED THE REST OF THE STATIONARY DISC WAS REMOVED WITHOUT DISSAMBLY OF THE BRAKE. THE INNER HALF OF THE MAIN WHEEL WAS SCORED BY THE BRAKE DISC AND WAS REPLACED ALONG WITH THE BRAKE ASSEMBLY. WHEN THE BRAKE WAS LAST REPAIRED THE DISC WAS EXAMINED AND FOUND TO BE SERVICABLE TO CONTINUE IN SERVICE WITHOUT REPLACING THE PADS. THEREFORE NDT WAS NOT REQUIRED. THE BRAKE HAD COMPLETED 963.2 HRS AND 851 CYCLES DURING THIS INSTALLATION.

CA041109003

BEECH

PWA  

PPG  

GROUND WIRE

BURNED

11/1/2004

1900D

PT6A67D

 

MS250852BB5

WINDSHIELD HEAT

(CAN) DURING CRUISE FLT AT FL210, THE FLIGHT CREW DETECTED AND ODOR FOLLOWED BY SMOKE EMANATING FROM THE DASH AREA. THEY DONNED MASKS AND REQUESTED PRIORITY LANDING . THEY RAN THRU THEIR EMERGENCY PROCEDURES AND AFTER THE WINDSHIELD HEAT WAS SELECTED OFF THE SMOKE DISSIPATED. AN UNEVENTFUL LANDING WAS COMPLETED AND AIRCRAFT BROUGHT TO MAINTENANCE. MAINTENANCE FOUND THAT THE GROUND WIRE HAD CONTACTED THE DASHBOARD EYEBROW AND THE HEAT HAD CAUSED IT TO SMOLDER. THE WIRE WAS REPLACED AND ROUTED TO ENSURE NO CONTACT CAN BE MADE WITH ANYTHING. A FLEETWIDE INSPECTION IS BEING CARRIED OUT AT THIS TIME AND WILL LEAVE SDR OPEN UNTIL TOTAL RESULTS.

CA040810002

BEECH

PWA  

 

FIRE LOOP

BROKEN

8/4/2004

1900D

PT6A67D

 

24412886

RT ENGINE

(CAN) CREW NOTED THAT THE RT FIRE LOOP WOULD NOT TEST. MAINTENANCE FOUND THE FWD FIRE WIRE LOOP PARTIALLY BROKEN PREVENTING CONTINUITY. THE WIRE WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

CA040713008

BEECH

PWA  

 

SEAL

TORN

7/12/2004

1900D

PT6A67D

 

1294000371

PAX DOOR

(CAN) DURING CRUISE FLIGHT THE CREW NOTED AN INCREASED NOISE FROM THE MAIN DOOR AND WAS UNABLE TO MAINTAIN CABIN PRESSURE APPROPRIATE FOR 170 ALTITUDE. THE AIRCRAFT WAS DESCENDED TO 100 AND THE FLIGHT CONTINUED TO DESTINATION. MAINTENANCE WAS DISPATCHED AND FOUND THE MAIN DOOR PRESSURE SEAL HAD TORN ALLOWING THE SEAL TO COLLAPSE. DEBRIS IN THE FORM OF GRAVEL WAS FOUND, WHICH MAY HAVE CONTRIBUTED TO THE SEAL FAILURE. THE SEAL WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

CA040629009

BEECH

PWA  

 

BOLT

UNDERTORQUED

6/28/2004

1900D

PT6A67D

 

 

VERTICAL STAB

(CAN) IN REFERENCE TO AN MAINTENANCE ALERT, AN INSPECTION WAS CARRIED OUT TO THE VERTICAL STABILIZER FRONT SPAR ATTACHMENT BOLTS FOR SECURITY AND TORQUE OF AIRCRAFT. ONE AIRCRAFT WAS FOUND WITH BOLT TORQUE UNDER THE SPECIFIED TORQUE ON THE RT SIDE UPPER AND LT SIDE LOWER. THE BOLTS WERE RE-TORQUED AND A CONTINUING INSPECTION WAS SET UP TO THE FLEET AT 1000 HOUR INTERVALS.

CA040927002

BEECH

PWA  

 

CROSS TIE

CRACKED

9/21/2004

200BEECH

PT6A41

 

97430000115

FUSLEAGE

(CAN) DURING MAINTENANCE, A CRACK WAS DISCOVERED IN A FUSELAGE CROSS TIE FOR THE UPPER RT FUSELAGE, IMMEDIATELY AFT OF THE EMERGENCY EXIT WINDOW. NEW PART HAS BEEN ORDERED AND WILL BE INSTALLED TO RECTIFY THIS DEFECT.

CA040422007

BEECH

PWA  

 

RECEPTACLE

BURNED

4/21/2004

200BEECH

PT6A41

 

2062071

CABIN

(CAN) WHEN THE CABIN CENTER HEADLINER WAS REMOVED DURING ROUTINE MX, RADIANT HEAT RECEPTACLES/SOCKETS WERE FOUND CHARRED AND MELTED WITH THE WIRE CONNECTERS INSIDE THE SOCKET LOOSE AND BURNT, PROBABLY FROM THE AMOUNT OF CURRENT BEING DRAWN THROUGH THE WIRES WHEN RADIANT HEAT WAS ON FOR LONG PERIODS OF TIME OVER THE YEARS OF OPERATION. RECEPTACLES, SOCKETS, AND CONNECTERS WERE REPLACED NEW ON BOTH THE FRONT AND BACK OF THE CABIN CENTER HEADLINER, AND FUNCTION TESTED SERVICEABLE. ALL OTHER KA 200 S OPERATED BY THE COMPANY WERE INSPECTED AND FOUND TO HAVE SIMILAR DAMAGE, TO SOME DEGREE ON THE RADIANT HEAT CONNECTERS. ALL PARTS WERE REPLACED NEW AND SYSTEMS CHECKED SERVICEABLE.

CA040423002

BEECH

PWA  

 

BULKHEAD

CORRODED

3/5/2003

200BEECH

PT6A41

 

 

FUSELAGE

DURING A SCHEDULED INSPECTION OF THE REAR PRESSURE BULKHEAD A LOCALIZED AREA OF PITTING CORROSION WAS DISCOVERED AROUND THE BULKHEAD FITTING FOR THE RELIEF TUBE CONNECTION. THE AREA WAS CLEANED AND INSPECTED AND AN APPROVED DOUBLER REPAIR CARRIED OUT. THE BULKHEAD FITTING ASSEMBLY WAS REPLACED WITH NEW TO PREVENT THE POSSIBILITY OF ANY FURTHER LEAKAGE. ALL OTHER AIRCRAFT IN THE FLEET WERE INSPECTED WITH NO DEFECTS NOTED.

2005FA0000031

BEECH

PWA  

 

CABLE

BROKEN

10/12/2004

400A

JT15D5

 

 

LT MLG

DURING SCHEDULED INSPECTION FOUND LT MAIN GEAR UPLOCK EMERGENCY EXTENSION CABLE BROKEN NEAR OB END. REPLACED CABLE WITH NEW PN128-380021-55 CABLE ASSEMBLY AND RIGGED IAW BE 400/400A, MM 32-30-00. ORIGINAL PN, PART TT NOT SUPPLIED, POSSIBLY ORIGINAL. ASSEMBLY PN FOR THIS SN RANGE AIRCRAFT HAS BEEN SUPERSEDED TWICE IAW CURRENT BE 400/400A IPC. APPEARS TO HAVE FAILED FROM AGE/TIME IN SERVICE. RECOMMEND ESTABLISHING A LIFE-LIMIT ON THIS CABLE ALSO, OR ISSUE A SB REQUIRING IMPROVED PN CABLE INSTALLATION. TTAF: 5397.4 HRS.

CA041115004

BEECH

PWA  

 

GENERATOR

INTERMITTENT

11/11/2004

99  

PT6A20

 

 

ELECTRICAL

(CAN) ON CLIMB OUT THE PILOT OBSERVED THAT ONLY ONE GENERATOR WAS ACCEPTING LOAD. DECIDED TO RETURN TO DEPARTURE AERODROME WITHOUT CARRYING OUT ANY CONFIRMATION CHECKS. A SUBSEQUENT MAINTENANCE INSPECTION DETERMINED THAT AT LIGHT ELECTRICAL LOADS BOTH GENERATORS DO NOT ALWAYS STAY ON LINE. BOTH GENERATORS WERE CONFIRMED TO BE WORKING. BOTH GENERATOR INDICATING SYSTEMS WERE CONFIRMED TO BE FUNCTIONAL.

CA040927007

BEECH

PWA  

 

DOOR

INOPERATIVE

9/24/2004

99  

PT6A20

 

50430043663

LT AFT FUSELAGE

(CAN) ON APPROACH, AT 20 MILES OUT AND 2500 FT ASL THE CABIN DOOR OPENED. FLIGHT SERVICES WAS INFORMED AND THE AIRCRAFT LANDED UNEVENTFULLY. THE COPILOT CLOSED THE DOOR AFTER LANDING. THE DOOR AND SURROUND WERE INSPECTED NO DAMAGE FOUND.

CA041122004

BEECH

PWA  

 

TIRE

BLISTERED

11/17/2004

A100

PT6A28

 

185F035

MLG 

(CAN) AFTER A PILOT REPORTED THAT THE NR 3 TIRE WAS FLAT, MAINTENANCE REPLACED THE WHEEL ASSY. DURING THE REMOVAL IT WAS NOTICED THAT THE IB SIDEWALL HAD A LARGE BLISTER. IT APPEARS THAT AN AREA (3 INCHES IN DIAMETER) OF THE OUTSIDE LAYER OF RUBBER (.0625 IF AN INCH THICK) WAS DISBONDED FROM THE REST OF THE TIRE, THE AIR PRESSURE CAUSED THIS TO INFLATE CREATING A LARGE BLISTER. THIS BLISTER EVENTUALLY RUBBED ON THE BRAKE CALLIPER CAUSING THE BLISTER TO BURST, DEFLATING THE TIRE.

CA040510006

BEECH

PWA  

 

FITTING

CRACKED

5/6/2004

A100

PT6A28

 

11561001S1

ELEVATOR TORQUE

(CAN) DURING A PHASE INSPECTION THE TAIL CONE WAS BEING REINSTALLED WHEN A CRACK WAS NOTICED ON THE LT TORQUE TUBE. THE CRACK EXTENDS FROM THE TAPER PIN HOLE TO THE EDGE OF THE FITTING. THESE FITTINGS ARE NDT EVERY 1000 HRS AND THIS TUBE WAS DONE AT 142.5 HRS.

CA041122011

BEECH

PWA  

 

O-RING

DISPLACED

11/16/2004

A100

PT6A28

 

 

FCU FUEL BOWL

(CAN) FUEL LEAK ON LT ENGINE IN FLIGHT. CAUSE BEING, DISPLACED O-RING ON FCU FUEL BOWL. VARIFIED BOWL HAD BEEN TORQUED TO SPECS IAW MM, CHAPTER 73-10-02 FOR ARGO-TECH PUMPS.

CA041130012

BEECH

PWA  

 

STARTER GEN

FAILED

11/29/2004

A100

PT6A28

 

23048018

LEFT 

(CAN) DURING CRUISE FLIGHT AT 12000 FEET THE PILOTS NOTICED THE LT GENERATOR FAIL LIGHT CAME ON. ALSO A PASSENGER INDICATED THAT HE NOTICED SPARKS COMING FROM THE ENGINE. THE GENERATOR WAS SELECTED OFF AND AIRCRAFT RETURNED TO BASE FOR INSPECTION. MAINTENANCE INSPECTED THE AIRCRAFT AND NOTICED THAT THE REAR BEARING IN THE STARTER GENERATOR HAD FAILED CAUSING IT TO SELF-DESTRUCT. THE GENERATOR WAS REPLACED, ENGINE WAS INSPECTED FOR DAMAGED AND AIRCRAFT WAS RETURNED TO SERVICE.

2004FA0000935

BEECH

 

 

SKIN

DELAMINATED

12/20/2004

B200

 

 

10140453S

LT WING

SKIN DELAMINATION ON LT WING CENTER SECTION UPPER SURFACE AFT OF THE SPAR NOTICED BY MAINTENANCE CREW, WHILE MAINTENANCE WAS BEING COMPLETED ON A NON-RELATED MATTER.

2004FA0000928

BEECH

 

 

STRINGER

CRACKED

12/21/2004

B200

 

 

1014400311

FUSELAGE

STRINGER NR 9 ON THE LT SIDE FOUND CRACKED DURING NON-RELATED MAINTENANCE.

2005FA0000025

BEECH

PWA  

 

BLOWER

ARCED

1/10/2005

B200

PT6*

 

1013841763

COCKPIT

PILOT REPORTED AN ELECTRICAL SMELL DURING FLIGHT AND THEN THE FORWARD VENTILATION BLOWER WENT INOPERATIVE. FOUND THE BRUSHES WORN OUT AND ARCING ON THE ARMATURE. REPLACED WITH OVERHAULED UNIT AND FUNCTIONAL CHECK OK.

CA040628008

BEECH

PWA  

 

SKIN

CRACKED

6/28/2004

B200

PT6A42

 

 

FUSELAGE

(CAN) COMBINATION VHF/GPS ANTENNA DOUBLER AND FUSELAGE SKIN CRACKED UNDER ANTENNA WHICH WAS ENGINEERED AND INSTALLED IAW LSTC NR C-LSA01-625/D. FUSELAGE REPAIRED AND ANTENNA REMOVED. NEW REPAIR DOUBLER INSTALLED.

CA040628009

BEECH

PWA  

 

SKIN

CRACKED

6/28/2004

B200

PT6A42

 

 

FUSELAGE

(CAN) COMBINATION VHF/GPS ANTENNA DOUBLER AND FUSELAGE SKIN CRACKED UNDER COMANT ANTENNA WHICH WAS ENGINEERED AND INSTALLED IAW LSTC NR C-LSA01-625/D. FUSELAGE REPAIRED AND ANTENNA REMOVED. NEW REPAIR DOUBLER INSTALLED.

2005FA0000034

BEECH

PWA  

 

RELAY

FAILED

10/19/2004

B200C

PT6A42

 

SM50D7

TE FLAPS

WHILE THE AIRCRAFT WAS IN FLIGHT, THE FLAPS FAILED TO EXTEND TO THE SELELCTED APPROACH POSITION. THE PILOT CYCLED THE FLAP SELECT SWITCH TO UP AD BACK TO APPROACH AND THE FLAPS EXTENDED. MAINTENANCE INVESTIGATED THE REPORTED PROBLEM AND WAS ABLE TO DUPLICATE THE PROBLEM ON THE GROUND. WHEN THE FLAPS WERE SELECTED TO APPROACH THE FLAPS MOVED APPROXIMATELY 5 DEGREES AND QUIT MOVING. AFTER ACCESS WAS GAINED TO THE FLAP MOTOR/GEARBOX AND RELAY, A TAP ON THE RELAY RETURNED THE FLAPS TO NORMAL SELECTOR SWITCH RESPONSE OPERATION. INSTALLATION OF A REPLACEMENT RELAY SOLVED THE PROBLEM. THE (FAILED ) RELAY HAD 69.0 HOURS. (WP19200503541)

AOC04006

BEECH

 

 

COMPRESSOR

DAMAGED

8/18/2004

B300C

 

 

1015552119

AIR CONDITIONER

PILOT REPORTED FREON AIR CONDITIONING SYSTEM INOPERATIVE FOLLOWING A FLIGHT. FOUND COMPRESSOR CLUTCH PLATE HAS SEPARATED FROM THE COMPRESSOR AND WAS FOUND IN THE LOWER ENGINE COWL. FIRE SLEEVE ON OIL LINE FROM THE OIL COOLER HAD IMPACT DAMAGE (SLEEVE CUT) BUT NO DAMAGE TO THE OIL LINE. NO OTHER DAMAGE NOTED.

CA041123001

BEECH

PWA  

 

PIN  

MISSING

11/19/2004

C90A

PT6A21

 

NAS427K6

ELEVATOR CONTROL

(CAN) THE PRIMARY CABLE FOR THE ELEVATOR CONTROL HAD JUMPED OUT OF THE PULLEY. THE (SPRING PIN) THAT PREVENTS THIS FROM HAPPENING WAS OUT OF POSITION (UNABLE TO STOP THE CABLE FROM LEAVING THE PULLEY). ABRASION OF THE ELEVATOR CABLE AT THE PULLEY AND ON SUPPORTING STRUCTURE A SHORT DISTANCE FROM WHERE THE ELEVATOR CABLE, EMERGES FROM THE PRESSURE VESSEL AS IT TRAVELS AFT TO THE BELLCRANK.

CA040713001

BEECH

PWA  

 

SHUTOFF VALVE

FAILED

7/12/2004

C90A

PT6A21

 

1013890253

FUEL SELECTOR

(CAN) FAILED FUNTIONAL TEST IAW PILOTS CHECK LIST. REPLACED

2005FA0000033

BEECH

CONT

 

RELAY

INTERMITTENT

11/5/2004

F33A

IO520*

 

SM50D7

DYNAMIC BREAKER

PILOT SELECTED GEAR DOWN AND NOTHING HAPPENED, SELECTED GEAR DOWN AGAIN AND GEAR CAME DOWN. ON FURTHER TROUBLESHOOTING FOUND RELAY WAS INTERMITTNET, PROBABLE CAUSE AT THIS TIME UNKNOWN, THIS IS SUPPOSE TO BE AN IMPROVED RELAY SO THERE IS NO RECOMMENDATIONS AT THIS TIME.

CA040811009

BELL

ALLSN

 

CLAMP

MISSING

7/26/2004

206B

250C20

 

 

TAIL ROTOR PEDAL

(CAN) ON DECENT PILOT FELT A TAP ON THE TAIL ROTOR PEDALS, AND LOOKED INTO HIS SLINGING MIRROR AND DETERMINED THAT THE LT BEAR PAW WAS MISSING. AFTER LANDING HE NOTICED DAMAGE TO TAIL ROTOR BLADES, AND VERTICLE FIN. ON INSPECTION, IT WAS FOUND THAT A CLAMP THAT WOULD PREVENT THE BEAR PAW FROM SLIPPING OFF WAS MISSING FROM THE INSTALLATION.

CA041223005

BELL

ALLSN

 

PITCH LINK

CRACKED

8/21/2004

206B

250C20B

 

206010355009

MAIN ROTOR

(CAN) DURING A SCHEDULED 100-HOUR INSPECTION TWO (2) VERTICAL CRACKS WERE FOUND ON A MAIN ROTOR PITCH LINK. THE CRACKS (APPROX. .180)

CA040615002

BELL

 

 

PIN  

IMPROPER PART

6/11/2004

206B1

 

 

206031620101

DOOR HANDLE

(CAN) CREW AND PASSENGER, INTERIOR (D) SHAPED DOOR HANDLES FOUND TO HAVE LOCKING (SPRING PINS) TOO SHORT INSTALLED BY THE MANUFACTURER. MS171525 (.438 INCH LONG) INSTALLED INSTEAD OF MS171526 (.500 INCH LONG).

CA041007004

BELL

ALLSN

 

GEAR

WORN

9/27/2004

206BELL

250C18

 

3579501200

OIL PUMP

(CAN) THIS IS THE OIL PUMP GEAR THAT DRIVES THE HYDRAULIC PUMP ON THE AC, GREASING INTERVAL IS 300 HRS. THIS SHAFT WAS GREASED EVERY 100 HRS AND HAS TOTALLY WORN OUT. THIS SHAFT ALSO WEARS OUT THE COUPLING IT ATTACHES TO, AS WELL.

CA041124009

BELL

ALLSN

 

DISC PACK

CRACKED

11/8/2004

206L

250C20R

 

327211

TAIL ROTOR DRIVE

(CAN) DISC PACK, 1 DISC CRACKED.

CA041123010

BELL

ALLSN

 

BYPASS SWITCH

CORRODED

11/3/2004

206L

250C20R

 

 

FILTER ASSY HEAD

(CAN) FILTER LIGHT CAME ON UPON LANDING. REMOVED FILTER AND INSPECTED. NO CONTAMINATION FOUND AND TEST LIGHT CIRCUIT. A LIGHT CAME ON AGAIN AND UPON INVESTIGATION, IT WAS FOUND THAT THE SWITCH WAS CORRODED. A NEW FILTER ASSY. WAS INSTALLED AND TESTED. IT FUNCTIONS CORRECTLY. INCIDENT HAPPENED 35 HOURS AFTER 300 HR INSP, WHICH INCLUDED FILTER CHANGE.

ALGA095160

BELL

 

 

BLADE

CORRODED

6/7/2004

206L1

 

 

206015001119

MAIN ROTOR

DURING ROUTINE A/F INSPECTION, CORROSION AND SEPARATION WAS NOTED ON LOWER SURFACE SKIN/SPAR INTERFACE IMMEDIATELY O/B OF GRIPFINGER. REPLACED W/SERVICABLE PART.

PG9R97953

BELL

ALLSN

 

FUEL NOZZLE

CRACKED

11/5/2004

206L1

250C28

 

6899001

ENGINE

FUEL NOZZLE SPRAY SHROUD CRACKED. A NEW MATERIAL SHOULD BE USED FOR THE SPRAY SHROUD. (K)

HEEA095226

BELL

ALLSN

 

ENGINE

STALLED

5/8/2004

206L3

250C30P

 

23004545

 

COMPRESSOR STALL WHILE HOVERING FOR TAKE OFF.

CA041007008

BELL

PWA  

 

CONTROL TUBE

CRACKED

10/7/2004

212  

PT6T3

 

212076101001

MAIN ROTOR

(CAN) WE ARE PRESENTLY DOING A 3000 HOUR AIRFRAME INSPECTION. THIS VERTICAL UPPER SERVO CONTROL TUBE WAS SENT TO A NDT SHOP FOR INSPECTION. THE NDT SHOP STATED THAT THEIR WAS A LONGDITUDANAL CRACK ON THE UPPER END OF CONTROL TUBE. SINCE THE LAST INSPECTION THE TUBE HAS 2617 HOURS ON IT. THE AIRFRAME TIME IS 28,644 HOURS.

CA040812003

BELL

PWA  

 

BULKHEAD

CRACKED

7/19/2004

212  

PT6T3

 

212030156047

TAILBOOM

(CAN) BULKHEAD FRAME CRACKED ADJACENT TO RT UPPER TAILBOOM ATTACH BOLT. FRAME REPLACED.

CA040407011

BELL

PWA  

 

TAPE

IMPROPER PART

4/7/2004

212  

PT6T3

 

 

GYROS

(CAN) ADHESIVE BACKED LEAD TAPE HAD BEEN USED TO BALANCE THE PITCH ERECTION VANES. IAW MANUFACTURER'S SERVICE ADVISORY NR 75, DATED JANUARY 25, 1985, LEAD TAPE SHOULD NOT BE USED TO BALANCE AIM GYROS AS IT CAN FALL OFF AND CAUSE THE GYRO TO BECOME INOPERATIVE.

CA040422004

BELL

PWA  

 

GRIP

BROKEN

4/18/2004

212  

PT6T3

 

2050010461

CYCLIC STICK

(CAN) DURING ROUTINE GREASING AND SERVICING OF MAIN ROTOR COMPONENTS AME ATTEMPTED TO MOVE THE PILOT'S CYCLIC STICK. AS THE MOVEMENT WAS ATTEMPTED, THE GRIP BROKE INTO TWO PIECES. THE FRACTURE OCCURRED BETWEEN THE FORCE TRIM RELEASE SWITCH AND CARGO RELEASE SWITCH. NEW GRIP WAS REWIRED AND INSTALLED. A/C RETURNED TO SERVICE.

ALGA098260

BELL

 

 

UNIVERSAL

WORN

12/6/2004

407  

 

 

406310405101

M/R DRIVE

UNIVERSAL BEARING HAS AXIAL PLAY BEYOND LIMITS. REPLACED WITH NEW BY FIELD MAINTENANCE.

ALGA098261

BELL

 

 

UNIVERSAL

WORN

12/6/2004

407  

 

 

406310405101

M/R DRIVE

UNIVERSAL HAS AXIAL PLAY BEYOND LIMITS. REPLACED WITH NEW BY FIELD MAINTENANCE.

CA041005004

BELL

 

 

HUB  

OVERSIZED

9/23/2004

407  

 

 

406012102109

TAIL ROTOR HEAD

(CAN) T/R HUB FOUND TO HAVE 1.6255 - 1.6260, INTERNAL DIAMETER FOR ELASTOMERIC FLAPPING BEARING INSTALL, OVERSIZE FROM .0002 TO .0007.

CA041104005

BNORM

LYC  

 

WHEEL

CRACKED

11/2/2004

BN2A

O540E4C5

 

16104700

MLG 

(CAN) CREW FELT LOSS OF BRAKE PRESSURE ON RT SIDE. RETURN TO RAMP. MAINT FOUND NR 3 IB WHEEL HALF BROKEN CAUSING BRAKE UNIT TO DETACH FROM BRAKE DISK. BRAKE UNIT FOUND ON TAXIWAY BY AIRPORT OPS. GIVEN TO TC OUTSIDE OF THEIR SOPS. LOCAL TC OFFICE, RETAINED POSSESSION OF BRAKE UNIT AND WILL NOT RETURN UNIT, DESPITE ENDEAVORS TO RETRIEVE FOR OWNER. THEREFORE UNABLE TO DETERMINE ORIGINAL CAUSE OF FAILURE WHETHER WHEEL HALF OR BRAKE UNIT FAILED FIRST.

CA040928001

BOEING

RROYCE

 

ENGINE

FAILED

9/12/2004

717200

BR700715A130

 

 

 

(CAN) IN FLIGHT SHUT DOWN AND AIR TURN BACK. IN CLIMB LOUD BANG AND TGT INCREASED TO 1000 DEG C. PILOT SHUT DOWN ENGINE AND RETURNED TO ORIGIN. ON GROUND, DEBRIS FOUND IN TAIL PIPE. ENGINE WILL BE INDUCTED IN OCTOBER. SUSPECT ED HPT BLADE FAILURE, FURTHER INFO WILL BE PROVIDED AT ENGINE STRIP.

CA040611005

BOEING

PWA  

 

SWITCH

INOPERATIVE

6/8/2004

727225

JT8D15A

 

10608197

KRUEGER FLAP

(CAN) AFTER TAKE OFF AND DURING CLIMB IT WAS OBSERVED THAT THE LT OB KRUGER FLAP WAS NOT RETRACTED. BOTH INDICATIONS SHOWED THE KRUGER WAS STILL EXTENDED. THE AIRCRAFT MADE AN UNSCHEDULED LANDING WITHOUT INCIDENT. JUMPER ASSY WAS INSTALLED IAW B727-27-80-02, L/E FLAP JUMPER CABLE INSTALLATION, AND CHECKED SERVICEABLE. THE AIRCRAFT WAS RELEASED FOR SERVICE. NO FURTHER PROBLEMS DURING SUBSEQUENT FLIGHT.

CA041123004

BOEING

PWA  

BOEING

HINGE

DAMAGED

11/22/2004

727233

JT8D15

 

69222825

DOOR HALF

(CAN) HYDRAULIC BAY DOOR SEPARATED FROM AIRCRAFT. AIRCRAFT WAS BEING POSITIONED FROM THE MAIN MAINTENANCE BASE ON THE MORNING OF NOVEMBER 22, 2004. DURING SERVICE CHECK BY MAINTENANCE, IT WAS NOTICED THAT THE HYDRAULIC BAY DOOR WAS MISSING. MAINTENANCE SUSPECT DOOR HINGE FAILURE. THE HYDRAULIC BAY STRUCTURE WAS INSPECTED FOR SECONDARY STRUCTURE DAMAGE. SERVICEABLE DOOR AND DOOR HINGE ASSY WAS INSTALLED AND AIRCRAFT WAS RETURNED TO SERVICE.

CA050119003

BOEING

PWA  

 

SWITCH

INTERMITTENT

1/19/2005

727233

JT8D15

 

H1010153

NLG 

(CAN) ON APPROACH, LANDING GEAR CYCLED DOWN FOR LANDING. THE NOSE LANDING GEAR RED INDICATOR STAYED ILLUMINATED AND NO GREEN INDICATION WAS SEEN. GEAR WAS RE-CYCLED AND THE GEAR WAS EXTENDED WITH PROPER INDICATION. MAINTENANCE LUBED THE NOSE GEAR AND JACKED THE GEAR AND CYCLED THE GEAR NUMEROUS TIMES, NO FAULTS FOUND. THE AIRCRAFT WAS DISPATCHED, NO FAULT ON LANDING THERE. THIS IS THE SECOND OCCURENCE AND SECOND SDR FOR THE SAME AIRCRAFT AND SNAG. DUE TO ITS HISTORY, NOSE GEAR DOWN POSITION SWITCH S93 AND THE NOSE GEAR LOCKED SWITCH S96 ARETO BE REPLACED BEFORE THE AIRCRAFT WILL BEDISPATCHED.POSSIBLE INTERNAL INTERMITTENT FAILURE TO ONE OF THE SWITCHES AND AT THE SAME TIME ALL WIRING WILL BE INSPECTED.

CA040812001

BOEING

PWA  

 

B-NUT

CRACKED

7/29/2004

727243

JT8D15

 

65178444440

HYDRAULIC LINE

(CAN) CREW REPORTED 'A' SYSTEM HYDRAULIC FLUID LOSS IN FLIGHT. MAINTENANCE FOUND LEAK AT B-NUT END FITTING AT 'A' SYSTEM MODULE. LINE REPLACED.

CA041001004

BOEING

CFMINT

 

ENGINE

FAILED

9/29/2004

737*

CFM567B22

 

 

NR 1 

(CAN) AIRCRAFT REPORTED STRONG ODOR THROUGHOUT THE CABIN AND FLIGHT DECK IN CLIMB. NO SMOKE VISIBLE. CREW RAN AIR CONDITIONING IN MANUAL/AIR MIX VALVES COLD, SMELL DISSIPATED. AIRCRAFT RETURNED TO DEPARTURE AND LANDED WITHOUT INCIDENT. NO EMERGENCY WAS DECLARED. MAINTENANCE CONDUCTED ENGINE RUNS ON BOTH ENGINES AT 70 PERCENT N2 FOR 10 MINUTES WITH EACH CORRESPONDING PACK RUNNING IN HOTMODE. ODOR DISSIPATED GRADUALLY. SYSTEM CHECKED SERVICEABLE. AIRCRAFT RETURNED TO SERVICE WITH NO FURTHER INCIDENTS TO REPORT. NOTE: PREVIOUS NIGHT MAINTENANCE INCLUDED NR 1 ENGINE FAN BLADE LUBE/INSPECTION TASK NR 95-072-00-01.

CA040412001

BOEING

 

ROSEMOUNT

PITOT LINE

LEAKING

4/6/2004

737200

 

 

 

PITOT TUBE ASSY

(CAN) B737-200 PITOT TUBE ASSEMBLY FAILED BENCH CHECK WITH A PITOT LEAK IN EXCESS OF 200 KTS/MIN. THE LEAK WAS DETERMINED TO BE ORIGINATING WHERE THE PITOT TUBE AIRFRAME ATTACHMENT CONNECTS TO THE BASE OF THE PITOT TUBE ASSEMBLY. THE COMPONENT WAS A USED PART ACQUIRED FROM A DISTRIBUTOR, QWEST AIR PARTS INC, IN MEMPHIS TN. THE PITOT TUBE HAD BEEN BENCH CHECKED SERVICEABLE BY CROSS-CHECK AVIATION, FAA REPAIR STATION XK8R253Y LOCATED IN RENO, NEVADA.

CA040412002

BOEING

 

ROSEMOUNT

PITOT LINE

LEAKING

4/6/2004

737200

 

 

 

PITOT TUBE ASSY

(CAN) B737-200 PITOT TUBE ASSEMBLY FAILED BENCH CHECK WITH A PITOT LEAK IN EXCESS OF 350 KTS/MIN. THE LEAK WAS DETERMINED TO BE ORIGINATING WHERE THE PITOT TUBE AIRFRAME ATTACHMENT CONNECTS TO THE BASE OF THE PITOT TUBE ASSEMBLY. THE COMPONENT WAS A USED PART ACQUIRED FROM A DISTRIBUTOR, QWEST AIR PARTS INC, IN MEMPHIS TN. THE PITOT TUBE HAD BEEN BENCH CHECKED SERVICEABLE BY CROSS-CHECK AVIATION, FAA REPAIR STATION NR XK8R253Y LOCATED IN RENO, NEVADA.

CA040412003

BOEING

 

ROSEMOUNT

PITOT LINE

LEAKING

4/8/2004

737200

 

 

 

PITOT TUBE ASSY

(CAN) B737-200 PITOT TUBE ASSEMBLY FAILED BENCH CHECK WITH A PITOT LEAK IN EXCESS OF 350 KTS/MIN. THE LEAK WAS DETERMINED TO BE ORIGINATING WHERE THE PITOT TUBE AIRFRAME ATTACHMENT CONNECTS TO THE BASE OF THE PITOT TUBE ASSEMBLY. THE COMPONENT WAS A USED PART ACQUIRED FROM A DISTRIBUTOR, QWEST AIR PARTS INC, IN MEMPHIS TN. THE PITOT TUBE HAD BEEN BENCH CHECKED SERVICEABLE BY CROSS-CHECK AVIATION, FAA REPAIR STATION NR XK8R253Y LOCATED IN RENO, NEVADA.

CA040412005

BOEING

 

ROSEMOUNT

PITOT LINE

LEAKING

4/8/2004

737200

 

 

 

PITOT TUBE ASSY

(CAN) B737-200 PITOT TUBE ASSEMBLY FAILED BENCH CHECK WITH A PITOT LEAK IN EXCESS OF 10 KTS/MIN. THE LEAK WAS DETERMINED TO BE ORIGINATING WHERE THE PITOT TUBE AIRFRAME ATTACHMENT CONNECTS TO THE BASE OF THE PITOT TUBE ASSEMBLY. THE COMPONENT WAS A USED PART ACQUIRED FROM A DISTRIBUTOR, QWEST AIR PARTS INC, IN MEMPHIS TN. THE PITOT TUBE HAD BEEN BENCH CHECKED SERVICEABLE BY CROSS-CHECK AVIATION, FAA REPAIR STATION # XK8R253Y LOCATED IN RENO, NEVADA.REF SDRS20040412001, 2004041202, AND 2004041203.

CA041110001

BOEING

PWA  

 

PROXIMITY SENSOR

FAILED

11/8/2004

737200

JT8D15

 

 

LE SLAT

(CAN) UPON SELECTION OF FLAPS 15 ON LANDING CHECKLIST THE L/E FLAP TRANSIT REMAINED ILLUMINATED AND THE NR 4 SLAT INDICATOR WAS SHOWING IN TRANSIT. REPLACED AND ADJUSTED NR 4 SLAT PROX SENSOR IAW MM 27-88-11. NR 4 SLAT FOUND DENTED ON UPPER SURFACE, REPLACED NR 4 SLAT IAW MM 27-81-21. RII CARRIED OUT. UPON FURTHER INVESTIGATION IT WAS FOUND THAT DAMAGE FROM A PREVIOUS BIRD STRIKE WAS FOUND TO THE SLAT CURTAINS WHICH CAUSED THE DAMAGE TO THE PROX SENSOR. THIS DAMAGE WAS NOT VISIBLE WITHOUT REMOVING L/E PANELS.

SROM200400056

BOEING

 

 

LIGHT

CORRODED

8/4/2004

737201

 

 

30043231

EXTERIOR

L2 DOOR EXTERIOR LIGHT INOP. REMOVED AND REPLACED L2 EXTERIOR EMERGENCY LIGHT IAW B737 M/M 33-51-61 - OPS CH'D GOOD.

CA041122013

BOEING

PWA  

 

SKIN

CRACKED

11/18/2004

737201

JT8D15

 

 

FUSELAGE

(CAN) A 4 INCH CRACK WAS FOUND ON THE OUTER FUSELAGE SKIN JUST AFT OF THE WING TO BODY FAIRING RT SIDE. CRACK LOCATED ON STR 15R (2) TWO INCHES AFT OF STA.727A. CRACK REPAIRED IAW SRM 53-30-3 FIG48 DETAIL XI TIMES 53851.20 CYCLES 46695.

SROM200400055

BOEING

 

 

BATTERY PACK

INOPERATIVE

6/20/2004

737205

 

 

20131A

EMERGENCY LIGHT

L2 DOOR EMERGENCY LIGHT INOP. CHANGED OUT BATTERY PACK. OPS CHECKED GOOD.

CA040510004

BOEING

PWA  

 

RING

DAMAGED

5/7/2004

737217

JT8D17

 

MS905820

FUEL FLOW TRANS

HAVE HAD SEVERAL OCCURRENCES OF FUEL LEAKS FROM THE JT8D FUEL FLOW TRANSMITTERS. THE LEAKS ARE EVIDENT AT VERY HIGH POWER SETTINGS. A FLEET CAMPAIGN HAS BEEN COMPLETED WHICH CHECKED ALL ENGINES FOR LEAKS AND RECTIFIED DEFECTS. AN EXTENSIVE INVESTIGATION IS BEING CONDUCTED BY OUR MAINTENANCE PROVIDER AND PRELIMINARY RESULTS SHOW THE CAUSE TO BE DEFECTIVE TEFLON BACK-UP RINGS MS9058-20. ALL STOCK OF THE SUSPECT PART HAS BEEN INSPECTED AND ANY DEFECTIVE BACK-UP RINGS FOUND HAVE BEEN QUARANTINED. OUR MAINTENANCE PROVIDER HAS CONTACTED THEIR SUPPLIER OF THE PART WITH THE FINDING. ADDITIONALLY THEY ARE CHECKING FOR OTHER APPLICATIONS FOR THE PART WITHIN THEIR VARIOUS FLEETS. A FULL REPORT WILL BE ISSUED AND I WILL UPDATE THIS SDR WITH ALL ADDITIONAL INFO WHEN THE REPORT IS AVAILABLE.

CA041105003

BOEING

PWA  

 

FIRE LOOP

INOPERATIVE

11/4/2004

737281

JT8D17

 

894093

NR 1 ENGINE

(CAN) ENGINE NR 1 FIRE WARNING AT 8000 ASL ON APPROACH. FIRE BOTTLES AND SQUIBS REPLACED IAW MM. NR 1 LOWER FIRE LOOP REPLACED AND CONNECTOR D1098 IAW MM. SYSTEM TESTED SERVICEABLE.

CA041201004

BOEING

PWA  

 

SKIN

CRACKED

11/29/2003

737296

JT8D9A

 

 

FUSELAGE

(CAN) TWO INCH CRACK WAS FOUND ON OUTER FUSELAGE BETWEEN STA 727A, 727B AT STR. 16L. FUSELAGE CRACK REPAIRED IAW SRM 53-30-3 FIG.48 SHEET 34 DETAIL XII. TIMES- 59472:22 CYCLES- 54285.

CA050111001

BOEING

PWA  

 

GUSSET

CRACKED

1/5/2005

7372Q9

JT8D9A

 

654581945

NLG 

(CAN) DURING A ROUTINE PHASE 3 CHECK (137.5 HRS.), A 2.75 INCH CRACK WAS FOUND ON THE NOSE LANDING GEAR GUSSET WHILE CARRYING OUT SERVICE DIFFICULTY ALERT AL-2002-03.RETRACT ACTUATOR SUPPORT FITTING GUSSET REPLACED IAW SRM 51-30-2 FIG II. TIMES. 61981.7 CYCLES. 52905.

CA040629006

BOEING

RROYCE

 

IDG  

FAILED

6/26/2004

757*

RB211535E437

 

73664E

RT GENERATOR

(CAN) RT GEN FAILED ON CLIMBOUT. COULD NOT RESET, QRH CARRIED OUT. AIRCRAFT RETURNED TO DEPARTURE. ETOPS DOWNGRADED TO 120MIN. OPERATE IAW MEL 24-00-1.

CA050114003

BOEING

RROYCE

 

MOTOR

LEAKING

1/12/2005

75728A

RB211535E437

 

887087

HYD ACTUATOR

(CAN) A/C DEPARTED AND TURNED AROUND AFTER NOTICING SLOW STEADY DECLINE IN CENTER SYSTEM QUANTITY. MAINTENANCE FOUND FLUID LEAKING FROM FUSELAGE DRAIN HOLES IN THS COMPARTMENT. UPON INVESTIGATION MAINTENANCE FOUND CENTER SYSTEM HYD MOTOR ON THIS GEARBOX LEAKING FLUID OUT MOTOR DRAIN LINE BUT MOST WAS COMING OUT THS GEAR BOX VENT HOLE ON FWD SIDE OF GEARBOX POSSIBLY DUE TO A PARTIALLY BLOCKED MOTOR DRAIN LINE. MFG INDICATED THAT WE WILL HAVE TO REPLACE THE THS ACTUATOR DUE TO THE HYDRAULIC FLUID LEAKAGE CONTAMINATING THE ACTUATOR GEAR BOX.

CA040920001

BOEING

PWA  

 

ACTUATOR

CORRODED

6/17/2004

767233

JT9D7R4D

 

251T43101

STABILIZER TRIM

(CAN) WATER INGRESS INTO GEAR BOX CAUSED EXTENSIVE CORROSION, INVESTIGATION ON GOING WITH MFG (STAB TRIM ACTUATOR).

2104

BOEING

GE  

 

ENGINE

VIBRATION

10/15/2004

767300

CF680C2B7

 

 

NR 1 

NR 1 ENGINE SHUT DOWN DURING FLIGHT DUE TO VIBRATION.

CA050111003

BOEING

GE  

 

OVEN

FIRE

1/11/2005

767375

CF680C2B6F

 

6253190003

MID GALLEY

(CAN) FAULT: JUST PRIOR TO DESCENT, SOMETHING WAS BEING COOKED IN THE MID CABIN GALLEY. AS THE F/A WAS ABOUT TO REMOVE IT, A FIRE WAS FOUND AT THE BACK OF THE OVEN. 3 FIRE EXT. WERE USED TO DOUSE THE FIRE. NO EMERGENCY WAS DECLARED, NO ADVERSE PAX REACTION. AIRCRAFT REMOVED FROM SERVICE, WIRING INSPECTION U/WAY.

CA050113003

BOMBDR

PWC  

 

PUMP

CRACKED

1/10/2005

DHC8400

PW150A

 

6617302

HYD SYSTEM

(CAN) NR2 HYDRAULIC SYSTEM FAILED DURING CLIMBOUT FROM BASE. PILOTS COMPLETED CHECKLIST AND PERFORMED AIR TURNBACK WITH UNEVENTFUL LANDING . PUMP HOUSING CRACKED WITH SUBSEQUENT FLUID LOSS INTO NACELLE. ENGINE DRIVEN PUMP REPLACED.

CA050113002

BOMBDR

PWC  

 

PUMP

MAKING METAL

1/9/2005

DHC8400

PW150A

 

6617302

NR 1 HYD SYSTEM

(CAN) DURING APPROACH TO BASE, NR 1 HYD ISO VLV AND NR 1 ENG HYD PUMP CAUTION LIGHT ILLUMINATED. NR 1 SYSTEM PRESSURE 0 PSI. STBY PRESS NORMAL AFTER SPU SELECTED ON. EMERGENCY LANDING DECLARED. AIRCRAFT STOPPED ON RUNWAY AND WAS TOWED IN. NR1 PROP COULD NOT BE ROTATED BY HAND. METAL FOUND IN CASE DRAIN AND PRESSURE FILTERS. REPLACED NR 1 EDP.

CA041125003

BOMBDR

PWC  

 

ECU  

FAILED

9/3/2004

DHC8400

PW150A

 

699018002

PROPELLLER

(CAN) AUTO FEATHER SYSTEM FAILED TO ARMED WHEN TAKE-OFF POWER WAS APPLIED. ABORTED TAKE-OFF. FAULT CODE 794 WAS LOGGED IN THE CENTRAL DIAGNOSTIC SYSTEM (CDS) DURING THE FOLLOWING OVERSPEED GOVERNOR TEST. A FUNCTIONAL TEST OF THE PEC AND CALIBRATION PROCEDURE WAS THEN PERFORMED IAW AMM TASK 61-20-36-720-801. FAULT CODE 238 REMAINED LOGGED IN THE CDS AS WELL AS PEC CAUTION LIGHT AND POWERPLANT MESSAGE ON THE ED AND FINALLY THE LT PROPELLER ELECTRONIC CONTROL UNIT (PEC) WAS REPLACED IAW AMM TASK 61-20-36.

CA040611001

BOMBDR

PWC  

 

SWITCH

BURNED

6/7/2004

DHC8400

PW150A

 

RV4NBYSD502A

READING LIGHT

(CAN) PILOT REPORTED BURNING SMELL IN THE COCKPIT. MAINTENANCE FOUND THE DIMMER SWITCH OF THE CO-PILOTS READING LIGHT BURNED THE SWITCH PN RV4NBYSD502A WAS REPLACED AND A FUNCTION CHECK CARRIED OUT. NO FURTHER PROBLEMS.

CA040610009

BOMBDR

PWC  

 

PUMP

FAILED

6/6/2004

DHC8400

PW150A

 

661732

NR 2 HYD SYSTEM

(CAN) DURING CLIMB FROM AIRPORT, NR 2 ENG HYD PUMP AND ASSOCIATED FLIGHT CONTROL CAUTION LIGHTS ALL ON HYD QTY 75 PERCENT. ACTIVATED PTU, THEN PRESSURE RETURNED TO NORMAL. AFTER LDG AND FLAPS SELECTED FOR LANDING, HYD QTY DECREASED TO 30 PERCENT. FLIGHT CONTROL C/LS ILLUMINATED AGAIN. CONTINUED LANDING WITHOUT FURTHER INCIDENT. STOPPED ON TAXIWAY FOR TOWING TO GATE, AT THAT TIME HYD QTY WAS 0 PERCENT. FOUND NR 2 EDP HANGER TRUNNION SCREWS, 1 MISSING AND 3LOOSE AND PACKING BLOWN OUT. REPLACED EDP.

CA040610006

BOMBDR

PWC  

 

BLADE

DEPARTED

6/9/2004

DHC8400

PW150A

 

 

COMPRESSOR

(CAN) AN AIRCRAFT CARRIED AN EMERGENCY LANDING AFTER EXPERIENCING A NR 2 ENGINE FIRE INDICATION. PRELIMINARY INFORMATION ADVISES LPC BLADE DEPARTURE AND COMPRESSOR SEIZURE. OIL WAS FOUND IN AND AROUND THE ENGINE AND NACELLE AREA AND HEAT DAMAGE WAS ALSO FOUND ON THE WIRING HARNESSES. FIRE BELIEVED TO HAVE BEEN CONTAINED WITHIN ENGINE. MFG INVESTIGATING THE ISSUE.

CA041124010

BOMBDR

PWC  

 

ACTUATOR

FAILED

8/30/2004

DHC8400

PW150A

 

3994001009

ELEV PITCH TRIM

(CAN) DURING DECENT INBOUND TO BASE, THE PITCH TRIM CAUTION LIGHT CAME ON, QRH PERFORMED AND IT BECAME APPARENT THAT WE HAD A FAILURE OF THE PITCH TRIM. ATC NOTIFIED AND THE APPROACH PLANNED WITH HIGH SPEED FOR AS LONG AS POSSIBLE. DURING SPEED REDUCTION STICK FORCES INCREASED SIGNIFICANTLY AS DESCRIBED IN QRH. STICK FORCES LIGHTENED ON SELECTION OF FLAP 5, AND INCREASED AGAIN WITH SPEED REDUCTION. ALTHOUGH QUITE HEAVY TO HOLD, THE APPROACH AND LANDING WERE PERFORMED WITHOUT PROBLEMS. ELEVATOR PITCH TRIM ACTUATOR WAS REPLACED IAW AMM TASK 27-32-06.

CA041125002

BOMBDR

PWC  

 

PROXIMITY SENSOR

FAULTY

11/10/2004

DHC8400

PW150A

 

82410888011

NLG 

(CAN) DURING DECENT TO BASE WITH LANDING GEAR RETRACTED, NOSE (GREEN), NOSE (RED) AND HANDLE (AMBER) LIGHT ILLUMINATED FOR ABOUT 3 MINUTES. EXTENSION, LANDING AND TAXI NORMAL. PSEU FAULT HISTORY INDICATED NGDN1 UNREASONABLE NEAR FAULT. REPLACED NGDN1 PROXIMITY SENSOR IAW AMM 32-61-06.

CA040422005

BOMBDR

PWC  

 

ACTUATOR

LEAKING

2/11/2004

DHC8400

PW150A

 

46455109

LT MLG

(CAN) AFTER GEAR DOWN SELECTION, NR 2 HYD ISO VALVE' CAUTION CAME ON AND DURING THE WHOLE APPROACH TO LANDING, 'OUTBOARD ROLL SPOILER CAUTION LIGHT' CAME ON INTERMITTENTLY. THIS WAS DUE TO, LOW QUANTITY IN NR 2 HYD SYSTEM. MADE A GO AROUND, AND KEPT GEAR DOWN WITH FLAPS 5. PERFORMED SYSTEM FAILURE CHECKLISTS AND DECIDED TO COMPLETE ALTERNATE GEAR EXTENSION PROCEDURE AS WELL. A NORMAL LANDING COMPLETED. INVESTIGATION/ACTION, EXTENSION HOSE FOR LT MAIN LANDING GEAR EXTENSION/RETRACTION ACTUATOR FOUND LEAKING. EXTENSION HOSE REPLACED ACCORDING AMM 32-31-11.

CA040422006

BOMBDR

PWC  

 

WIRE

SHORTED

2/17/2004

DHC8400

PW150A

 

 

NLG PROX SENSOR

GEAR OUT INDICATION AFTER TAKEOFF, NOSE GEAR DOWN, NOSE GEAR UNSAFE AND GEAR IN TRANSIT LIGHT REMAINED ON. DURING DESCENT, THE LIGHTS WENT OUT AND ON FOUR TIMES. INVESTIGATION/ACTION, THE PROXIMITY SENSOR ELECTRONIC UNIT INTERROGATED FOR FAULTS, PSEU FAULT NR 1. THE NOSE GEAR DOWN SENSOR WIRING WERE FOUND SHORTED. SENSOR REPLACED ACCORDING AMM 32-61-06.

CA041124006

BOMBDR

PWC  

 

PUMP

INOPERATIVE

11/23/2004

DHC8402

PW150A

 

6617302

HYD SYSTEM

(CAN) DURING CLIMB, 10 MIN. AFTER TAKE OFF, CLOSE TO 25 000 FT, PILOT NOTICED NR 2 ENGINE HYD PUMP CAUTION LIGHT FOLLOWED BY A LOSS OF NR 2 HYD FLUID QTY ON COCKPIT GAUGE. PILOT FOLLOWED Q400 QUICK REF HANDBOOK PROCEDURE NR 12.5. PTU HAS BEEN MANUALLY SELECTED ON WITH NO PRESSURE INCREASE IN NR 2 SYST DUE NO HYD FLUID, PTU SELECTED OFF, NR 2 HYD ISOLATION VALVE SELECTED ON. AC RETURNED AND ALTERNATE LANDING GEAR EXTENSION PROCEDURE USED. NR 2 ENGINE DRIVE HYD PUMP R & R IAW AMM. NR 2 HYD SYS BLEED IAW AMM AND NR 2 HYD SYS SERVICE IAW AMM. AC RETURN TO MAINT BASE. ENGINE DRIVE HYD PUMP DETAIL FINDING REPORT WILL FOLLOW.

2005FA0000010

BRAERO

GARRTT

 

CLAMP

CRACKED

12/7/2004

HS125700A

TFE7315R

 

FIOA5SCP2013

TAIL PIPE

THE DEFECT IS A FATIGUE CRACK, CAUSED BY BEING OVERSTRESSED DUE TO LOAD LIMITS, POSSIBLE OVERTORQUED. MAYBE THIS PART SHOULD BE MADE STRONGER, TO HANDLE THE STRESS. THIS DEFECT WAS FOUND BY A PENETRANT INSPECTION. THE LOCKING NUT NEEDS TO BE REMOVED, IN THIS CASE THE DEFECT WOULD NOT HAVE BEEN NOTICED IF THE LOCKING NUT HAD NOT BEEN REMOVED. (CE09200501913) (K)

CA040611007

BRAERO

RROYCE

 

DEICE SYSTEM

INOPERATIVE

5/30/2004

HS7482A

DART5342

 

 

RIGHT

(CAN) RT ENGINE DE-ICE FOUND INOPERATIVE, RETURNED TO DEPARTURE, STA NR 2 RELAY P/N CZ105648-2 REPLACED ENGINE INLET DE-ICE RING COWL REPLACED. HARNESS, P/N 6V10659 REPLACED FUNCTION TEST, SERVICEABLE

CA041202006

BRAERO

RROYCE

 

ENGINE

FAILED

12/2/2004

HS7482A

DART5342

 

 

RIGHT

(CAN) AC WAS ENROUTE, WHILE IN CRUISE THE AC YAWED TO THE RT AND THE STBD ENGINE SPOOLED DOWN. IN-FLIGHT SHUTDOWN PROCEDURE WAS CARRIED OUT AND THE AC RETURNED, WHERE AN UNEVENTFULL LANDING WAS MADE. UNTIL THE ENGINE SHUT DOWN, OPERATING INDICATION WERE NORMAL. MAINTENANCE INSPECTION REVEALED HEAVY STEEL CONTAMINATION OF THE OIL FILTERS, INCLUDING A COMPLETE CROWN FROM A GEAR WHEEL. INITIAL INVESTIGATION INDICATES THE PROPELLER GEAR BOX FAILED.THIS ENGINE IS DUE FOR OVERHAUL AND THE ENSUING STRIP REPORT WILL FURNISH A MORE IN DEPTH REPORT.

CA040803001

BRAERO

RROYCE

 

BATTERY

INOPERATIVE

7/23/2004

HS7482A

DART5342

 

 

MASTER

(CAN) AFTER DEPARTURE, THE CREW OBSERVED THAT THE STBD CHARGE RATE WAS NOT DECLINING BELOW 10 AMPS. THE AIRCRAFT RETURNED TO POINT OF DEPARTURE. MAINTENANCE REPLACED THE STBD BATTERIES AND THE AIRCRAFT WAS RETURNED TO SERVICE.

CA050119007

BRAERO

RROYCE

 

LANDING GEAR

UNKNOWN

1/5/2005

HS7482B

DART5342

 

 

 

(CAN) ON TAKEOFF, THE LANDING GEAR WOULD NOT RETRACT AFTER BEING SELECTED. THE AIRCRAFT RETURNED TO POINT OF DEPARTURE AND LANDED NORMALLY. THE AIRCRAFT WAS HANGARED AND A GEAR SWING CARRIED OUT, THE FAULT COULD NOT BE DUPLICATED. THE AIRCRAFT WAS RETURNED TO SERVICE.

CA050119009

BRAERO

RROYCE

 

HEATER

FAILED

1/12/2005

HS7482B

DART5342

 

S200 

CABIN

(CAN) SHORTLY AFTER DEPARTING, THE CABIN HEATER FAILED. THE CREW RETURNED THE AIRCRAFT TO POINT OF DEPARTURE. THE HEATER UNIT WAS REPLACED AND THE AIRCRAFT RETURNED TO SERVICE.

CA041130004

CESSNA

CONT

 

LINE

WORN

11/16/2004

150L

O200A

 

040031178

OIL PRESS

(CAN) THE OIL PRESSURE LINE UNDER THE INSTRUMENT PANEL WAS CHAFED AGAINST THE CABIN HEATER CONTROL CABLE. WE REPLACED THE PRESSURE LINE AND INSTALLED IT CORRECTLY.

CA040610010

CESSNA

CONT

 

LINE

CORRODED

6/10/2004

150M

O200A

 

040031158

FUEL SYSTEM

(CAN) FUEL LINE ASSEMBLY LOCATION/LOCATED UNDER FLOOR AND UNDER CENTER CONSOLE. THIS LINE IS DIRECTLY FORWARD OF THE BELLY DRAIN. IT IS UP STREAM FROM THE GASCOLATOR AND DOWN STREAM OF THE FUEL SHUT-OFF. FUEL SMELL WAS DETECTED. FUEL STAINING WAS PRESENT. THE LINE PASSES THROUGH A BULKHEAD. THE LINE IS PROTECTED BY A GROMMET WHICH WAS INTACT. THE LINE HAD BECOME CORRODED AND PITTED AROUND THE GROMMET AREA AND DEVELOPED A PIN HOLE LEAK. LINE WAS REPLACED.

CA040422003

CESSNA

LYC  

 

MOUNT

CRACKED

4/22/2004

152  

O235L2C

 

045100336

ENGINE

(CAN) AT INSPECTION THE ENGINE MOUNT WHICH ALSO HAS PROVISION FOR MOUNTING THE NOSE LANDING GEAR WAS FOUND DAMAGED. TWO TUBES WERE CRACKED, THREE OTHERS WERE SLIGHTLY BENT. ALL EVIDENCE POINTS TO A UNREPORTED HARD LANDING. AIRCRAFT HAS BEEN THOROUGHLY INSPECTED FOR FURTHER DAMAGE. NONE FOUND.

2005FA0000026

CESSNA

CONT

 

CONTROL PANEL

WORN

1/13/2005

172  

O300*

 

 

PITCH CONTROL

AIRCRAFT WAS SUBSTANTIALLY DAMAGED DURING A LANDING ACCIDENT. PILOT WAS UNABLE TO FLARE AIRPLANE. DURING A POST ACCIDENT INSPECTION BY FAA INSPECTORS, IT WAS DISCOVERED THAT THE AIRPLANE'S CONTROL TEE PULLEYS FOR THE AILERON SYSTEM WOULD GET (HUNG UP) ON THE RADIO TRAY ASSEMBLY, WHEN THE CONTROL WHEEL TUBE WOULD REACH HALF TRAVEL. THE CONTROL TEE PIVOT AND THE LEFT INSTRUMENT PANEL CONTROL TUBE BALL SOCKET, EXHIBITED WEAR, AND THE CONTROL TEE COULD BE MOVED LATERALLY ALONG A PORTION OF THE CONTROL TEE PIVOT BOLT. ADDITIONALLY, THE RADIO-MOUNTING TRAY DID NOT INCLUDE THE INSTALLATION OF A VERTICAL SUPPORT TO HELP ASSURE PROPER CLEARANCE BETWEEN THE TRAY AND THE CONTROL TEE ASSEMBLY.

CA040506003

CESSNA

LYC  

 

TORQUE LINK

CRACKED

2/6/2004

172K

O320E2D

 

04425061

NLG 

(CAN) DURING INSPECTION, IT WAS DISCOVERED THE UPPER TORQUE LINK PART NUMBER 0442506-1WAS CRACKED. NEW PART WAS INSTALLED.

CA041103005

CESSNA

LYC  

 

PUSHROD

BROKEN

10/25/2004

172M

O320E2D

 

05170281

LT DOOR LATCH

(CAN) LT DOOR WOULD NOT OPEN AND CLOSE PROPERLY.

CA041122003

CESSNA

LYC  

 

GASKET

SPLIT

11/19/2004

172M

O320E2D

 

71973

INTAKE FLANGE

(CAN) INTAKE FLANGE GASKET SPLIT THROUGH CIRCUMFERENCE RESULTING IN MINOR VACUUM LEAK. THE GASKET MATERIAL IS HARD AND BRITTLE, AND APPEARS TO BE ERODING ON THE INNER EDGE. THIS IS THE FOURTH GASKET FOUND SPLIT IN THE LAST FEW WEEKS. THREE ON THIS ENGINE (1164 HOURS) AND ONE ON ANOTHER AT 700 HOURS. BOTH MGF FACTORY REMANUFACTURES. SUSPECT DEFICIENCY IN MATERIAL.

4356

CESSNA

LYC  

 

STARTER

DESTROYED

12/21/2004

172P

O320D2J

 

EBB131A

ENGINE

ON ENGINE START, STARTER BENDIX DID NOT DISENGAGE. ALL BENDIX DRIVE ENGAGEMENT TEETH SHEARED AND DAMAGED ENGINE STARTER RING GEAR. TIME SINCE OVERHAUL BY KELLY AEROSPACE 195.0

CA041129011

CESSNA

LYC  

CESSNA

COUPLING

BROKEN

11/27/2004

172P

O320D2J

 

C3010020211

ACTUATOR

(CAN) STUDENT AND INSTRUCTOR WERE PERFORMING A WALK AROUND OF THE AIRCRAFT BEFORE GOING FOR A LESSON. STUDENT SELECTED FLAPS DOWN THEY STARTED TO GO DOWN THEN THE FLAPS STOPPED MOVING BUT THE MOTOR KEPT RUNNING. FLAP MOTOR WAS REMOVED AND IT WAS FOUND THAT THE COUPLING BETWEEN THE MOTOR AND THE ACTUATOR HAD BROKEN. NEW COUPLING WAS INSTALLED AND THE FLAPS WORKED CORRECTLY.

CA041130011

CESSNA

LYC  

 

CONTROL UNIT

FAILED

11/22/2004

172R

IO360L2A

 

AC2101

ALTERNATOR

(CAN) ALTERNATOR FIELD C/B TRIPPED WHEN ALTERNATOR TURNED ON. ZERO VOLTS FOUND AT ALT FIELD TERMINAL. REPLACED ALTERNATOR CONTROL RELAY, NO CHANGE. REPLACED ALTERNATOR CONTROL UNIT, VOLTAGE AT FIELD TERMINAL OF ALTERNATOR. ALTERNATOR FUNCTIONING NORMALLY DURING GROUND RUNUP.

CA040629007

CESSNA

LYC  

AERO

CAPACITOR

CHAFED

6/25/2004

172R

IO360L2A

 

S19151

ALTERNATOR

(CAN) INTERMITTANT OCCURRENCE OF ALTERNATOR FAILING TO STAY ON LINE. INCORRECT POSITIONING OF CAPACITOR ALLOWED UNIT TO CHAFE AGAINST ENGINE BAFFLING UNTIL INTERNAL PORTION WAS EXPOSED CAUSED INTERMITTENT SHORT.

2005FA0000099

CESSNA

 

 

BULKHEAD

CRACKED

12/15/2004

172S

 

 

05522311

SPINNER

DURING A 100 HR INSPECTION THE FORWARD SPINNER BULKHEAD WAS FOUND TO BE CRACKED AROUND 4 OF THE 6 BOLT HOLES. THINK THAT THE CAUSE OF THE PROBLEM IS THAT THE TORQUE OF THE PROP WAS RAISED AND THE NEW TORQUE IS NOT ENOUGH TO CAUSE THE BULKHEAD AROUND THE BOLT HOLES TO BE PULLED INTO THE CHAMFERED AREA OF THE PROPELLER BOLT HOLES. THIS STRESSES THE BULKHEAD AND ALLOWS CRACKS TO START. TO PREVENT THIS PROBLEM POSSIBLY CONSIDER MAKING THE BULKHEAD OF THICKER MATERIAL OR REDESIGNING THE PART SO THAT WHEN IT IS TORQUED THERE IS STRESS RELIEF AROUND THE BOLT HOLES SO THAT THE BULKHEAD SITS FLAT. (K)

2005FA0000032

CESSNA

LYC  

 

BULKHEAD

CRACKED

12/1/2004

172S

IO360B1E

 

05522311

SPINNER

DURING 100 HRS INSPECTION, FOUND FWD BULKHEAD OF THE SPINNER CRACKED 4 PLACES AROUND PROPELLER BOLT HOLES. RECOMMENDATION: BULKHEAD MATERIAL STRONGER OR THICKER. (WP07200507539)

CA040610008

CESSNA

LYC  

CESSNA

BULKHEAD

BROKEN

6/9/2004

172S

IO360L2A

 

055032111

PROP SPINNER

(CAN) THE CORNER SECTION OF SPINNER AT LEADING EDGE OF PROPELLER BLADE CUT-OUT BADLY BENT (PEELED BACK) BY CENTRIFUGAL FORCE. THIS WAS CAUSED BY THE ADJACENT CORNER SECTION OF THE BACKPLATE (AROUND ANCHOR NUT) BREAKING OFF DURING OPERATION. NEW BACKPLATE DESIGN USED. (MOST CURRENT PN 0550321-12)

CA040615004

CESSNA

CONT

CONT

ROCKER BOSS

BROKEN

6/10/2004

180  

O470K

 

 

CYLINDER EXHAUST

(CAN) ROCKER BOSSES BROKE OFF, FOR ROCKER SHAFT ON EXHAUST VALVE.

CA041108005

CESSNA

CONT

 

SKIN

CORRODED

11/1/2004

180C

O470L

 

07310041

VERTICAL STAB

(CAN) VERTICAL STABILIZER REMOVED TO ACCESS FUSELAGE SIDE SKIN REPLACEMENT (COSMETIC) WITH STABILIZER ON WORKBENCH, VISIBLE ACCESS TO INTERNAL STRUCTURE REVEALED CONSIDERABLE SURFACE CORROSION EVERY WHERE INTERNALLY. EXTERNAL UNIT LOOKS FINE. RECOMMEND REMOVAL OF VERTICAL AND HORIZONTAL STABILIZERS ON A REGULAR BASIS. IE. 400 HRS/5 YEARS.

CA040730007

CESSNA

CONT

 

TRIM SYSTEM

CONTAMINATED

7/27/2004

180H

O470R

 

 

ELEV TRIM WHEEL

(CAN) ELEVATOR TRIM WHEEL WOULD ONLY MOVE .5 INCH. FOUND DEBRIS CONSISTING OF GRASS, PEANUT SHELLS ETC. A SQUIRRELS NEST JAMMING THE CHAIN (CABLE ATTACHED TO CHAIN) ON THE GEAR WHICH ACTIVATES THE WORM GEAR TO MOVE THE ELEVATOR UP AND DOWN. BECAUSE OF THE LOCATION UNDER THE CENTER OF THE ELEVATOR, BETWEEN TWO BULKHEADS. IT WAS DIFFICULT TO REMOVE. IT WAS COMPLETELY (ALL) REMOVED, USING MIRRORS, VACUUM CLEANER. ALL PARTS WHERE IN EXCELLENT CONDITION.

CA040506002

CESSNA

CONT

EDOAIREXXXXX

BAR  

CRACKED

4/19/2004

180H

O470R

 

3665710

FLOATS

DURING A ROUTINE, CHANGE OVER FROM SKIS TO FLOATS, IT WAS DISCOVERED THAT THE FORWARD SPREADER BAR ASSEMBLY PART NUMBER 36657-10 WAS BADLY CORRODED AND CRACKED. THE SPREADER BAR ASSEMBLY WAS REMOVED FROM EDO 249-2870 FLOATS. NEW PART NUMBER 26-32096 INSTALLED IN ACCORDANCE WITH STC SA00066SE AND INSTALLATION GUIDE FORAEROCET 26-32096 SPREADER BAR REPLACEMENT DOCUMENTA-10013.

2005FA0000101

CESSNA

LYC  

 

EXHAUST VALVE

SEIZED

7/12/2004

182T

IO540AB1A5

 

LW19001

NR 3 CYLINDER

UPON TAKEOFF, PILOT REPORTED POWER LOSS AND ROUGH RUNNING ENGINE. INVESTIGATION FOUND NR 3 CYLINDERS EXHAUST VALVE SEIZED. THIS WAS 4TH OCCURENCE SINCE NEW (1999). INSTITUTED 300 HOUR VALVE GUIDE REAM AND 25 HOUR OIL CHANGE. MFG DENIED REQUEST TO INCREASE VALVE GUIDE CLEARANCE.

CA040421003

CESSNA

PWA  

CESSNA

CARD

BROKEN

4/20/2004

208  

PT6A114A

 

 

DIRECTIONAL GYRO

(CAN) THE CO-PILOT'S DIRECTIONAL GYRO WAS RECENTLY REPLACED WITH THE ABOVE MENTIONED OVERHAULED INSTRUMENT. UPON COMPLAINT FROM PILOT, THE INSTRUMENT WAS HARD TO SET, A FUNCTIONAL TEST WAS COMPLETED. IT WAS FOUND THAT PUSHING THE KNOB IN AND TURNING IT DID NOT ROTATE THE CARD WITH EASE. FOUND THAT IT TOOK ABNORMALLY GREAT AMOUNT OF INWARD PRESSURE WHILE TURNING THE KNOB TO GET ANY MOVEMENT OF THE CARD ESPECIALLY IN THE CLOCKWISE ROTATION. THE INSTRUMENT HAS ONLY 37.6 HOURS AND 34 CYCLES SINCE OVERHAUL.

CA040810005

CESSNA

PWA  

 

SHIMMY DAMPENER

BROKEN

7/19/2004

208B

PT6A114A

 

26430096

MLG 

(CAN) SHIMMY DAMPENER BARREL END ENTIRELY BROKE OFF AT CIRCLIP GROOVE. ALL FLUID LOST,CIRCLIP MISSING, BROKEN PIECE MISSING. NO EVIDENCE OF PRIOR OVERSTEER.

CA040614004

CESSNA

PWA  

 

BELLCRANK

MISMANUFACTURED

6/10/2004

208B

PT6A114A

 

262400724

AILERON

(CAN) DURING COMPLETION OF MFG BULLETIN CAB03-4 ONE WELD WAS FOUND TO BE MISSING. THE MISSING WELD WAS ON THE LOWER ARM INNER SURFACE DESCRIBED AS ITEM 6 IN FIGURE 1 OF CAB03-4. ALL OTHER WELDS WERE PRESENT AND THE BELLCRANK SHOWED NO OBVIOUS DAMAGE OR DISTORTION CAUSED BY THE MISSING WELD.

CA040423003

CESSNA

CONT

 

SPRING

SEIZED

4/23/2004

210L

IO520L

 

12416432

MLG DOWNLOCK

DOWNLOCK SPRING ASSY SLIDING ACTION WAS RESTRICTED BY ACCUMULATION OF DIRT AND DEBRIS. DOWNLOCK WAS UNABLE TO FULLY ENGAGE RESULTING IN AN 'UNSAFE' GEAR IND. INSPECT REVEALED WET LUBRICATION ATTRACTED DEBRIS AND DIRT IN THE SPRING ASSY CONCENTRIC SLEEVE AND SPRING. CESSNA INSPECTION MANUAL SECTION 2 IS VAGUE REGARDING LUBRICATION TYPE AND APPLICABILITY AND STATES IN PART - 'AND ANY OTHER FRICTION POINT OBVIOUSLY REQUIRING LUBRICATION'. CONFUSION MAY ARISE IN THIS EXAMPLE. SUBMITTER RECOMMENDS A DRY LUBRICATION IN THIS AREA, AND INCREASED AWARENESS IN INDIVIDUAL INSPECTION PROGRAMS FOR A/C OPERATING IN 'OFF AIRPORT' LOCATIONS, GRAVEL AND DUSTY STRIPS. SUBMITTER'S A/C IS MODIFIED BY STC SA 5737SW NO DOOR KIT. AT LEAST 5 OTHER EXAMPLES EXIST IN A 14 YEAR SDR DATABASE SEARCH. SUBMITTER HAS INCLUDED ADDITIONAL TRAINING FOR FLIGHT AND GROUND PERSONNEL OPERATING AND MAINTAINING THIS A/C AND INCORPORATED ADDITIONAL DOCUMENTATION AND TRAINING DOCUMENTATION REFLECTING THIS CONDITION.

CA040423004

CESSNA

CONT

 

CYLINDER

CRACKED

4/23/2004

210L

IO520L

 

653446

ENGINE

CYLINDER CRACKED THROUGH 75 PERCENT OF CIRCUMFERENCE AT CYLINDER CROWN FROM A POINT BEYOND THE UPPER SPARK PLUG HOLE, AROUND THE EXHAUST VALVE, AND TERMINATING AT A POINT BEYOND THE LOWER SPARK PLUG HOLE (BUT NOT TRANSECTING THE HOLE).

CA040730005

CESSNA

CONT

 

CRANKCASE

CRACKED

5/23/2004

337D

IO360C

 

 

ENGINE

(CAN) ENGINE OIL LEAK DETECTED ON REAR ENGINE SUCTION INSPECTED FOUND 1.5 INCH LONG CRACK IN CASE BETWEEN NR 3 AND NR 5 CYLINDER. NO OTHER REPORTED DAMAGE. ENGINE REMOVED.

CA040930006

CESSNA

 

 

PAD  

MISSING

9/24/2004

402B

 

 

P5855BSW

PROP DEICE

(CAN) AFTER FLIGHT, PILOT SAW ON RT PROPELLER, ONE PROP DE-ICE PAD MISSING ON ONE BLADE. AFTER INSPECTION OF THE DEFECT, WE SAW THE GLUE WAS NOT HARD. THE DE-ICE PAD WAS INSTALLED AT O/H SHOP WITH NEW KIND OF GLUE. WE REMOVED THE OLD GLUE AND REINSTALLED A NEW DE-ICE PAD WITH CONTACT GLUE (3M 1300L). AIRCRAFT RETURNED TO SERVICE AFTER REPAIR.NOTE: IT'S NOT THE FIRST TIME THIS PROBLEM APPEAR DUE TO THIS NEW KIND OF GLUE.

CA041006005

CESSNA

CONT

 

LINE

CORRODED

9/22/2004

414  

TSIO520N

 

5100106236

LT ENG OIL

(CAN) PILOT AND AME FLYING HOME TO BASE OBSERVED THE LT ENGINE OIL PRESSURE DECREASING AT A SLOW RATE, UNTIL DECISION MADE TO SHUT DOWN THE ENGINE AND LAND AT THE NEAREST AIRFIELD. INVESTIGATION ON THE GROUND REVEALED OIL TO BE LEAKING FROM THIS LINE. LINE REPLACED AND CONDITIONS RETURNED TO NORMAL. CONTINUED ON HOME. NO FURTHER ACTION REQUIRED.

2004FA0000914

CESSNA

CONT

CONT

ROCKER

BROKEN

10/22/2004

421  

GTSIO520D

 

6399576

NR 3 CYLINDER

ANNUAL PRE-INSPECTION RUN-UP RAN GOOD. POST INSPECTION RUN-UP RAN ROUGH. SUSPECTED A STICKING VALVE. FURTHER INVESTIGATION REVEALED A BROKEN EXHAUST ROCKER ARM AND STUCK VALVE FOR NR 3 CYLINDER ON THE LEFT ENGINE. ALSO, NOTED IS AN APPARENT INCLUSION IN THE BROKEN ROCKER ARM.

1538T001

CESSNA

 

 

TABLE

MISINSTALLED

11/26/2004

421B

 

 

863422

CABIN

INSPECTED RIGHT HAND CABIN EXECUTIVE TABLE AT THE RECOMMENDATION OF ANOTHER MAINTENANCE FACILITY MAINTAINING SAME TYPE OF AIRCRAFT. FOUND A LEFT HAND TABLE INSTALLED. FORWARD CUP HOLDER WAS SCREWED TO THE TABLE MAKING EMERGENCY EXIT REMOVAL DIFFICULT. EMERGENCY EXIT CHECKED AT LAST TWO ANNUAL INSPECTIONS WITH THE INTERIOR REMOVED.

2004FA0000927

CESSNA

CONT

 

BRACKET

MISINSTALLED

12/21/2004

421B

GTSIO520C

 

51310103

ZONE 300

COMPLIED WITH MFG MEB 00-4 RUDDER BEARING INSPECTION/REPLACEMENT. FOUND RUDDER LOWER HINGE BEARING BRACKET INSTALLED UPSIDE DOWN FROM FACTORY. REPLACEMENT PROCEDURE DESCRIBED IN MEB FOUND ERRONEOUS AND INADEQUATE TO COMPLETE SATISFACTORY REPLACEMENT OF BRACKET. MS 2047AD4-11 AND AD 5-11 RIVETS CALLED OUT IN MEB ARE OF THE INADEQUATE LENGTH. THIS WILL REQUIRE -12 OR -13 LENGTH RIVETS. REPLACEMENT PN 5131010-3 IS NOT SAME SIZE AS ORIGINAL AND DOES NOT APPEAR TO HAVE ADEQUATE EDGE DISTANCE FROM RIVET HOLES AS WELL AS CAUSING BULGING OF VERTICAL STABILIZER SKINS BECAUSE IT IS SLIGHTLY TOO WIDE. A MAJOR RE-WRITE OF THIS MEB AND ITS COMPLIANCE INSTRUCTIONS IS NEEDED.

CA050118005

CESSNA

CONT

 

LANDING GEAR

COLLAPSED

1/17/2005

421C

GTSIO520L

 

 

RIGHT

(CAN) RT LANDING GEAR COLLAPSED ON LANDING, THIS IS A PRELIMINARY REPORT MORE INFORMATION WILL FOLLOW.

CA041110019

CESSNA

GARRTT

 

SUPPORT BRACKET

CRACKED

11/8/2004

441  

TPE33110

 

57150021

BELLCRANK

(CAN) AILERON BELLCRANK SUPPORT BRACKET WAS DISCOVERED TO BE CRACKED. PART WAS REPLACED WITH A NEW BRACKET AND THE AIRCRAFT RETURNED TO SERVICE.

2005FA0000098

CESSNA

PWA  

GOODYEAR

HEAT SHIELD

DAMAGED

11/7/2004

500CESSNA

JT15D1

 

5004549E

LT MLG TIRE

PILOT REPORTED, HE HAD HIT AN OBJECT ON RUNWAY DUE TO IMPACT SOUND HEARD ON LT SIDE OF AC AND BRAKE ANTI-SKID FAIL INDICATION. INVESTIGATED LT WHEEL AREA AND DISCOVERED THAT TIRE HEAT SHIELD HAD PARTIALLY DISLOGED FROM WHEEL ASSY. INSPECTED AREA AND FOUND PART OF HEAT SHIELD HAD TORN AWAY CUTTING BRAKE ANTI-SKID WIRE HARNESS, BENDING GEAR DOOR ROD, AND DENTING IB AREA OF LT LANDING LIGHT HSG. INSPECTED RT TIRE HEAT SHIELD AND FOUND IT LOOSE ALSO. INSP FOUND RT SHIELD TO BE INSTALLED CORRECTLY IAW MFG MM. DECISION WAS MADE TO REPLACE RT SHIELD. TIRE HEAT SHIELD HAS NOT HARD MOUNT ATTACHMENT TO WHEEL ASSY. UPGRADING AC TO NEW STYLE WHEEL/BRAKE ASSY IS THE ONLY VIABLE FIX TO PREVENT THIS FROM HAPPENING.

CA040810007

CESSNA

PWA  

BFGOODRICH

DISK

BROKEN

8/6/2004

550  

JT15D4

 

1338932

BRAKE STATOR

(CAN) WHILE PUSHING THE AIRCRAFT WITH A TUG THE LT BRAKE LOCKED UP. ON INSPECTION IT WAS DISCOVERED THAT ONE OF THE STATOR DISKS HAD BROKEN AND JAMMED THE BRAKE. THE BRAKE WAS REPLACED WITH AN OVERHAULED UNIT. AD2004-09-05 WHICH ADDRESSES MFG BRAKE STATORS BREAKING HAD BEEN ACCOMPLISHED RECENTLY AND PASSED THE INSPECTION AS CALLED OUT. BOTH STATORS ARE STAMPED 'CHANGE D', SO NO FURTHER ACTION WAS REQUIRED. IN LIGHT OF THIS INCIDENT THE REPLACEMENT CRITERIA SHOULD POSSIBLY BE CHANGED.

CA040730004

CESSNA

PWA  

BFGOODRICH

STATOR

CRACKED

7/27/2004

550  

JT15D4

 

1338931

BRAKE SYSTEM

(CAN) DURING TAXI PILOT NOTICED MORE THRUST THAN NORMAL WAS NEEDED TO TAXI AND AIRCRAFT WAS DIFFICULT TO TURN TO THE RT. MAINTENANCE INSPECTION DISCOVERED CRACKED STATOR WHICH WARPED CAUSING BRAKE TO BIND UP.

CA041130001

CESSNA

PWA  

 

COUPLER

DISCONNECTED

11/28/2004

550  

JT15D4

 

CM357024

CABIN PRESSURE

(CAN) COUPLING DISCONNECTED WHEN AIRCRAFT WAS AT FLIGHT LEVEL AND AIRCRAFT AT A OPERATING CABIN PRESSURE ALTITUDE. AIRCRAFT CABIN LOST PRESSURIZATION.

2004FA0000871

CESSNA

 

 

BRIDAL CABLE

FRAYED

8/1/2004

560CESSNA

 

 

6565007197CR

ELEVATOR

ELEVATOR AUTO PILOT BRIDAL CABLE FRAYED TO THE POINT OF LOCKING UP CONTROL. DURING LOCATING CONTROL BLOCKAGE CABLE BROKE COMPLETELY INTO AT THE SUPPORT GUIDE PULLEYS. PRE-SB 560-27-07.

CA041007006

CESSNA

PWA  

 

SLEEVE

WORN

9/22/2004

560CESSNA

JT15D5

 

7423461

THROTTLE CABLE

(CAN) DURING GROUND RUN OPERATIONS CHECK AFTER STARTER GENERATOR CHANGE THROTTLE WAS ADVANCED TO 70 PERCENT THEN RETARDED TO IDLE QUICKLY (1 SEC.). ENGINE FLAMED OUT. ENGINE RIGGING WAS CHECKED, THEN THE INNER CABLE OF THE AFT THROTTLE CABLE WAS REMOVED AND INSPECTED. FOUND THAT THE OUTSIDE SLEEVE ASSEMBLY COULD BE REMOVED EVEN WITH THE LOCK BOLT TIGHT AND THAT THE INNER CABLE WAS BEING PULLED OUT WHEN THE THROTTLE WAS QUICKLY RETARDED TO IDLE.

CA041126001

CESSNA

PWA  

 

CABLE

BROKEN

11/22/2004

560CESSNA

PW535A

 

656014131

TE FLAPS

(CAN) AC DEPARTED, DURING CLIMB THE PILOTS NOTICED THAT THE FLAP INDICATOR DID NOT MATCH FLAP SELECTOR HANDLE. FLAP POSITION WAS VERIFIED VISUALLY BY CO-PILOT PRIOR TO RETURNING TO BASE. UPON MAINTENANCE INVESTIGATION IT WAS FOUND THAT THE FWD FLAP FOLLOW-UP CABLE WAS BROKEN AT THE PULLEY SWEDGED BALL. SL560-27-11 (SWEDGED BALL INSPECTION) WAS ACCOMPLISHED APRIL26/04 AT 573.1 A/F HOURS 411 LDGS. THIS SB WAS NEXT DUE AT 873.1 HRS. AIRCRAFT TT AT FAILURE WAS 846.3 HRS (-26.8 HRS TO NEXT INSPECTION) THE CABLE WAS REPLACED, RIGGED IAW MM, DUAL INSPECTION C/W AND RETURNED TO SERVICE.

CA040830006

CESSNA

PWA  

 

PLUG

LEAKING

7/9/2004

560CESSNA

PW535A

 

49330

MAIN WHEEL

(CAN) MAIN WHEEL/TIRE ASSEMBLY LEAKING AIR 2-4 PSI PER DAY. REPLACED THERMAL RELIEF PLUG ASSEMBLY. THIS IS THE SECOND PLUG ASSEMBLY TO BE REPLACED ON THIS WHEEL (THERE ARE THREE PLUGS PER WHEEL ASSEMBLY).

CA040830004

CESSNA

PWA  

 

PANEL

INOPERATIVE

8/3/2004

560CESSNA

PW535A

 

7511001915

AUDIO CONTROL

(CAN) FRONT PANEL OF AUDIO CONTROL UNIT DOES NOT ILLUMINATE ON NIGHT SETTING.

2004FA0000872

CESSNA

 

 

BRAKE

OUT OF ADJUST

8/9/2004

650  

 

 

6242020519

MLG 

ON DEPARTURE FROM MKE, CREW NOTED A SHIMMY IN THE NOSE WHEEL AND ABORTED TAKEOFF. INSPECTION FOUND NOSE GEAR FRICTION BRAKE DRAG LOW. ADJUSTED FRICTION BRAKE PER CE650 MM. COMPLETED HIGH SPEED (100 KTS) TAXI CHECK WITH NO SHIMMY EVIDENT. RELEASED AIRCRAFT FOR SERVICE. (M)

CA040629008

CESSNA

LYC  

 

PLUG

WORN

6/17/2004

A152

O235L2C

 

LW11625

PISTON PIN

(CAN) A FEW PIECES OF NON-FERROUS MATERIAL WERE FOUND AT 1375.8 HOURS. FILTER RE-INSPECT SCHEDULED. SUBSEQUENT FILTER INSPECTION SHOWED HEAVY CONTAMINATION. ALL CYLINDERS REMOVED, FOUND PISTON PINS AND PLUGS NOT FLOATING. TWO PLUGS WERE WORN EXTENSIVELY. ALL PISTONS REMOVED FOR INSPECTION AND CLEANING, NO DAMAGE NOTED TO CYLINDER WALLS. PISTONS RE-INSTALLED WITH NEW PLUGS. ACCESSORY DRIVE COVER AND SUMP REMOVED FOR INSPECTION AND CLEANING. NO FURTHER EVIDENCE OF CONTAMINATION FOUND. NO FURTHER DAMAGE FOUND.

CA041001011

CESSNA

CONT

 

MAGNETO

ARCED

9/13/2004

A185F

IO520D

 

6310 

RIGHT

(CAN) PILOT REPORTED A 200 RPM DROP ON RT MAGNETO. TROUBLESHOOTING REVEALED THAT TOP IGNITION WIRE ON NR 5 CYLINDER WAS UNSERVICEABLE. WHEN HARNESS WAS REMOVED FROM MAGNETO, EVIDENCE OF HEAVY ARCING WAS NOTED IN THE NR 5 LEAD OUTLET AREA OF THE DISTRIBUTOR BLOCK.

CA040506001

CESSNA

CONT

 

SPAR

CRACKED

11/21/2003

A185F

IO520D

 

07326031

HORIZONTAL STAB

REMOVED HORIZONTAL STABILIZER. REAR SPAR REINFORCEMENT PART NUMBER 0732603-1 CHANGED. AFT ATTACHEMNT POINT REINFORCEMENT BRACKET RT PART NUMBER 0732101-4 REPLACED WITH NEW. ADJACENT RIVETS REPLACED. SERVICE KIT SK185-27 INSTALLED TO FACILITATE SCREW JACK REMOVAL. LT TRIM JACK REMOVED. NEW SCREW PART NUMBER 0712500-11 INSTALLED. TRIM JACK REINSTALLED. RIGGED AND SAFETIED AS PER CESSNA MANUAL.

CA040421004

CESSNA

CONT

 

PAN  

CORRODED

4/21/2004

A185F

IO550D

 

07520144

COWL FLAP

(CAN) DURING RIGHT COWL FLAP HINGE REPLACEMENT, FOUND COWL FLAP PAN ASSEMBLY HAS SEVERE CORROSION UNDER HINGE HALF. THIS AREA IS ONLY VISIBLE AFTER REMOVING THE HINGE.

2005FA0000024

CESSNA

CONT

 

BOLT

LOOSE

1/17/2005

T210M

TSIO520R

 

 

WASTEGATE VALVE

3 OF THE 4 BOLTS THAT ATTACH THE METAL PLATE THAT THE ACTUATOR IS MOUNTED ON TO THE WASTEGATE BODY WERE MISSING. FOURTH BOLT WAS BACKED OUT ABOUT HALF WAY. ALL THREE BOLTS FOUND LOOSE IN ENGINE COMPARTMENT. WASTEGATE ASSEMBLY ONLY 287 FROM OVERHAUL BY MAIN TURBO.THESE BOLTS ARE NOT EASILY OBSERVABLE AND REQUIRE A MIRROR TO SEE. RECOMMEND INSPECTION AT EACH OIL CHANGE AND TIGHTEN AS NEEDED.

CA040930002

CESSNA

CONT

 

SKIN

CRACKED

9/29/2004

T337G

TSIO360CB

 

14220006

LT WING

(CAN) DURING INSPECTION, CRACKS WERE DISCOVERED AT THE IB END OF THE LT AND RT UPPER OB WING SKINS WHERE THEY UNDERLAP THE FUEL TANK BAY COVERS. THE CRACKS ARE LOCATED IN THE RADIUS OF CUTOUT AREAS IN THE SKINS WHERE THE STINGERS JOIN AT WING STATION 150.0. THE AIRCRAFT IS EQUIPPED WITH FLINT WING TIP FUEL TANKS THAT WERE INSTALLED APPROXIMATELY 800 HOURS AGO. IT IS NOT KNOWN IF THIS IS A CONTRIBUTING FACTOR.

CA040927008

CESSNA

LYC  

CESSNA

PIVOT ASSY

CRACKED

9/27/2004

TR182

O540L3C5

 

224110213

MLG 

(CAN) RT BRAKE CONTINUALLY LOOSING FLUID. CENTER SECTION AT GEAR PIVOTS ALWAYS WET. BRAKE SWIVEL NOT LEAKING. PIVOT ASSEMBLY REMOVED AND CHECKED BY DYE PENETRATE INSPECTION FOUND TO BE CRACKED. INSTALLED NEW PIVOT ASSEMBLY IAW MAINTENANCE MANUAL.

CA040823BB

CESSNA

 

 

FITTING

CRACKED

8/20/2004

U206B

 

 

1216012

FUSELAGE

(CAN) DURING THE 100 HOUR INSPECTION THE RH MAIN GEAR OUTBOARD FITTING WAS FOUND CRACKED AT THE UPPER AFT RADIUS OF THE FITTING OPENING.THE FITTING WAS REPLACED IN ACCORDANCE WITH CESSNA'S RECOMMENDATIONS (OBTAINED FROM CESSNA) WITH A USED SERVICEABLE CUSTOMER SUPPLIED UNIT AFTER NDT INSPECTION.

CA041125004

CESSNA

CONT

CESSNA

BOLT

SHEARED

10/25/2004

U206C

IO520F

 

NAS464P5A42

NLG STRUT

(CAN) BOLT SHEARED ON LANDING CAUSING NOSE GEAR TO PIVOT FORWARD. NOTE: THIS BOLT WAS LAST CHANGED SEPTEMBER 9/94 AT 2875 I.T.T. (AIRCRAFT PRESENT TT IS 6238.7 HOURS) THIS AIRCRAFT HAS OPERATED ON SKIS (SUSPECT THAT BOLT WAS OVERSTRESSED IN THIS CONFIGURATION). THIS BOLT WAS CRACKED PRIOR TO FAILURE AS HALF OF FRACTURE IS BLACK AND TOTAL FAILURE IS WHITE. SOME DAMAGE TO AIRFRAME WAS ENCOUNTERED. IT SHOULD BE NOTED THAT INSPECTION OF THIS BOLT IS NOT REPLACED IN INSPECTION SCHEDULE.

CA040630002

CESSNA

CONT

 

CRANKCASE

CRACKED

6/30/2004

U206G

IO520F

 

 

ENGINE

(CAN) DURING UNSCHEDULED MAINTENANCE 3 CRACKS WERE NOTICED ON CRANKSHAFT NEAR PROP FLANGE. TWO CRACKS WERE APPROXIMATELY 2 INCHES IN LENGTH PARALLEL TO EACH OTHER WITH SMALLER CRACKS EXTENDING. ONE CRACK IS ALSO APPROXIMATELY 2 INCHES IN LENGTH AND ABOUT 1 INCH FROM THE OTHER TWO CRACKS. THESE CRACKS RUN ALONG THE CIRCUMFERANCE OF THE CRANKSHAFT.

CA040924007

CESSNA

CONT

 

TUBE

CRACKED

9/13/2004

U206G

IO520F

 

537296

PUSHROD

(CAN) NR 5 CYLINDER PUSH ROD TUBE HOUSINGS FOUND 1 CRACKED, AT CYLINDER HEAD END, THE OTHER WAS BENT AT OB END OF SPRING RETAINER.

24331

CIRRUS

 

 

BOLT

CHAFED

11/2/2004

SR22

 

 

AN334

ALT AIR DOOR

THE BOLT (P/N AN3-34) THAT SERVES AS THE PIVOT FOR THE ALTERNATE AIR DOOR IN THE INDUCTION DUCT ASSEMBLY (P/N 15708-001) IS BEING CHAFFED BY THE INDUCTION DUCT SUPPORT BRACKET (P/N 15671-002). IN ADDITION TO THE CHAFFED BOLT THE INDUCTION DUCT ASSY IS SUSCEPTIBLE TO CRACKING. ALSO INSPECTED 14 OTHER AIRCRAFT WITH COMPARABLE TIME OR LESS AND FOUND SIGNS OF CHAFFING AND/OR INDUCTION DUCT CRACKING REQUIRING REPLACEMENT OF THE INDUCTION DUCT ASSY. THIS CONDITION IS VERY DIFFICULT TO INSPECT WITHOUT REMOVING THE INDUCTION DUCT ASSY.

2005FA0000018

CIRRUS

CONT

 

OIL COOLER

CRACKED

11/11/2004

SR22

IO550N

 

654585

ENGINE OIL

THIS AIRCRAFT HAS HAD AN OIL COOLER REPLACED FOR THE SAME DEFECT AT

2201092004

CIRRUS

CONT

CIRRUS

BOLT

CHAFED

10/4/2004

SR22

IO550N

 

AN334

INDUCTION DUCT

DURING REMOVAL AND REPLACEMENT OF THE P/N 15708-001 INDUCTION DUCT ASSY IT WAS NOTED THAT DUCT WAS CRACKED IN THE AREA OF THE AN3-34 BOLT THAT SERVES AS THE HINGE POINT FOR THE ALTERNATE AIR DOOR. AFTER REMOVING THE BOLT IT WAS FOUND TO BE CHAFFED ALL THE WAY AROUND THE SHANK (360 DEGREES). IT APPEARS THE INDUCTION DUCT SUPPORT BRACKET P/N 15671-002, MADE OF STAINLESS STEEL, IS WEARING IT'S WAY INTO THE BOLT SHANK. SEVERAL OTHER AIRCRAFT WERE INSPECTED AND WERE FOUND TO HAVE BOLT WEAR AND/OR CRACKING OF THE DUCT IN THE SAME AREA. THE CRACKING OF THE DUCT IS VERY DIFFICULT TO SEE WITHOUT REMOVING THE ASSY AND THE CHAFFING OF THE BOLT CANNOT BE SEEN WITHOUT REMOVING IT.

CA040510002

CNDAIR

 

 

FRAME

CRACKED

5/3/2004

CL2151A10

 

 

21531036212

WING TO BODY

WHILE PERFORMING AD CF-1997-07R2 A CRACK WAS DISCOVERED BY EDDY CURRENT ABOUT ONE AND A HALF INCHES LONG ON THE OUTBOARD RT REAR WING TO FUSELAGE FRAME ANGLE. THE CRACK BECAME VISUALLY APPARENT AFTER BEING DETECTED BY NDT. THE CRACK STARTED AT THE TOP OF FRAME P/N 215-31036-212 AND EXTENDED PASS THE FIRST HIGH LOCK AND ON TOWARDS THE SECOND. THE AD WAS PERFORMED AT AIRFRAME TIME 1984.2 AND TOTAL WATER DROPS 6843 WHICH IS PRIOR TO THE COMPLIANCE REQUIREMENTS OF AD CF-1997-07R.

CA040630007

CNDAIR

PWA  

 

INDICATOR

DEFECTIVE

6/28/2004

CL2151A10

CA3  

 

21550724

PRESS TRANSMITER

(CAN) AFTER TAKE-OFF, THE RT FUEL PRESSURE INDICATOR WAS 1 PSI LOWER THAN PREVIOUS FLIGHTS. THE CREW ELECTED TO PROCEED FOR MAINTENANCE. AFTER CRUSING FOR AWHILE THEY NOTICED ANOTHER DROP IN FUEL PRESSURE AND ELECTED TO SHUT DOWN THE RT ENGINE. THEY LANDED SAFELY FOR MAINTENANCE. MAINTENANCE CHECKED THE RT FUEL SYSTEM FOR LEAKS AND NONE WERE FOUND. THE FUEL PRESSURE INDICATING SYSTEM WAS CHECKED AND THE TRANSMITTER WAS FOUND DEFECTIVE. THE TRANSMITTER WAS REPLACED AND GROUND CHECKED SERVICABLE. THE A/C WAS RETURNED TO SERVICE.

CA040825006

CNDAIR

PWA  

 

CASE

LEAKING

8/11/2004

CL2151A10

CA3  

 

177770

RT ENGINE

(CAN) AFTER A DROP DURING FIRE BOMBING OPERATIONS, THE CAPTAIN AND FO PERFORMED ENGINE VISUAL CONDITION CHECK. THE FO NOTED A LARGE AMOUNT OF OIL LEAKING FROM THE RT ENGINE. OIL TEMPERATURE, PRESSURE AND QUANTITY WERE CLOSELY MONITORED ON THE 20 MIN. FLIGHT BACK TO THE MAINTENANCE BASE. MAINTENANCE FOUND OIL LEAKING FROM AN INSERT ON THE FRONT NOSE CASE. THE NOSE CASE WAS REPLACED AND THE A/C RETURNED TO SERVICE.

CA040629010

CNDAIR

PWA  

 

MAIN BEARING

FAILED

6/29/2004

CL2151A10

CA3  

 

 

RT ENGINE

(CAN) WHILE CLIMBING AWAY FROM A WATER SCOOP, THE CREW NOTICED THAT THE RT ENGINE WAS BECOMING UNCONTROLLABLE, ROUGH RUNNING AND LOSING POWER. THE CREW DROPPED THE LOAD AND SHUTDOWN THE RT ENGINE AND FEATHERED THE PROPELLER. THE AIRCRAFT MADE THE SINGLE ENGINE LANDING WITHOUT INCIDENT, AND THE AIRCRAFT RETURNED TO THE HANGER FOR INVESTIGATION.

CA040510003

CNDAIR

PWA  

 

CONTROL CABLE

CORRODED

5/3/2004

CL2151A10

R2800*

 

215903812

RUDDER CONTROL

DURING A STRUCTURAL REPAIR TO THE RT REAR WING-TO-FUSELAGE FRAME ANGLE A PANEL AT WS 60.80, ADJACENT TO REAR SPAR, HAD TO BE DRILLED OFF TO FACILITATE THE REPAIR. IT WAS AT THIS TIME CORROSION WAS DISCOVERED ON THE RUDDER/AILERON INTERCONNECT CABLE P/N 215-90381-2 WHICH LIES DIRECTLY UNDER THIS PANEL. THE CORROSION WAS REMOVED AND UPON A CLOSER INSPECTION SEVERAL BROKEN STRANDS WERE NOTICED. THE MM WAS CONSULTED AND IT WAS DETERMINED THAT THE CABLE WAS BEYOND LIMITS. THE CABLE WAS REMOVED AND REPLACED WITH A SERVICEABLE UNIT AND THE WING PANEL WAS SEALED WITH AN APPROVED SEALANT. ITS WORTH NOTING THAT THE DAMAGE WOULD BE IMPOSSIBLE TO SPOT HAD IT NOT BEEN FOR THE REMOVAL OF THE RIVETED PANEL. THIS IS AN AREA NORMALLY INACCESSIBLE.

CA050120003

CNDAIR

PWA  

 

FITTING

BROKEN

1/20/2005

CL2156B11415

PW123

 

215T2429080

RUDDER

(CAN) THE RUDDER GEAR/TRIM TAB UPPER FITTING FOUND BROKEN ON A VISUAL INSPECTION. A/C 1655, HOURS 1054, CYCLES 7200 DROPS.

CA040507003

CNDAIR

 

 

HEATER

SMOKE

4/30/2004

CL6002B19

 

 

 

WINDSHIELD

DURING CRUISE, SMOKE FROM LEFT WINDOW HEATER. WHEN LT WINDSHIELD HEAT WAS TURNEDOFF, SMOKE STOP. DIVERTED FLIGHT. FOUND LOOSE SCREW AND DAMAGED TERMINAL LUG ON LEFT WINDSHIELD HEAT ELEMENT. LUG REPLACED AND SCREW TIGHTENED.

2004FA0000870

CNDAIR

 

 

ANGLE

CRACKED

7/30/2004

CL6002B19

 

 

601R35031239

FUSELAGE

FLOOR SUPPORT ANGLE AT FS 621, WL 73 OUTBOARD OF LBL AND RBL 27 CRACKED. REPAIR IAW BOMBARDIER AEROSPACE EO NR 601R-53-61-117.

CA040811002

CNDAIR

GE  

 

CONTROL UNIT

FAILED

7/29/2004

CL6002B19

CF343A1

 

47259701

NR 1 ENGINE

(CAN) FLT DIVERTED, EMERGENCY DECLARED. ON CLIMBOUT RECEIVED NUMEROUS FIRE FAIL MSGS., CAUTION MSG, THEY ALL DISAPPEARED. WE THEN RECEIVED A LH ENG FIRE WARNING AND WE SHUT DOWN NR 1 ENGINE. ON APPROACH WE RECEIVED A RH ENGINE FIRE WARNING MSG, ON LANDING WE RECEIVED A APU FAIL MSG, WHICH DISCHARGED THE BOTTLE. MTCE R/R THE FIREX CONTROLLER AND APU FIRE BOTTLE.

CA041129014

CNDAIR

GE  

 

PUMP

CRACKED

11/29/2004

CL6002B19

CF343A1

 

848847

HYDRAULIC SYS

(CAN) FAULT: ON CLIMB OUT MSP, CREW RECEIVED PAX DR HANDLE LATCH MSG, FOLLOWED BY HYD SYS 3 LOW PRESS. MSG FOLLOWED BY PAX DR WARNING MSG. ON AIR RETURN, ON APPROACH FLT, RECEIVED GEAR DISAGREE MSG AND CARRIED OUT MNL EXTENSION. FOUND LINE LEAKING ON PUMP 3B. FOUND CASE CRACKED ON PUMP 3A. REPLACED BOTH 3A AND 3B HYD. PUMP REPLACED PRESS/RETURN AND CASE DRAIN FILTERS SYS. 3. REPLACED HYD. LINE ON PULSE DAMPENER PUMP 3B. HYD SYST. SERVICED.

CA040613001

CNDAIR

GE  

 

IDG  

INOPERATIVE

6/11/2004

CL6002B19

CF343B1

 

755469D

NR 1 

(CAN) NR 1 IDG CAUTION MESSAGE CAME ON DURING TAKEOFF ROLL AND CREW ELECTED TO REJECT TAKEOFF. ON WEEK PRIOR OR(JUNE 5), THE CREW RECEIVED A CAUTION MESSAGE (DURING CRUISE AT 31000 FEET) ON EICAS FOR APPROX 30 SECONDS WITH SYNOPTIC CHANGING FROM GREEN TO YELLOW WHILE THE OUTPUT VOLTAGE REMAINED STEADY. MAINTENANCE CARRIED OUT A VISUAL INSPECTION AND THEN AS THE SNAG REOCCURRED, INITIALLY THE SYSTEM WAS DEFERRED IAW AS MEL PROCEDURE AND IDG WAS REPLACED AT THE SAME NIGHT HOURS SINCE INSTALLATION OF IDG. TT 2555.34 AND 1576 CYCLES ON A 381 DAY PERIOD.

CA040811003

CNDAIR

GE  

 

NOSE COWL

DAMAGED

7/25/2004

CL6002B19

CF343B1

 

22850080158

NACELLE

(CAN) PILOT REPORTED LOUD NOISE AND SOME LOSS OF ENGINE POWER ON THE RT ENGINE AT CRUISE. UPON LANDING, THE TOWER INFORMED THE AIRCRAFT THAT A COWLING FELL OFF AT LANDING. ENGINE LOWER NOSE COWLING PANEL WAS RECOVERED.MTC LOOKED AT THE AIRCRAFT AND FOUND THE RT ENGINE UPPER AND LOWER NOSE COWLINGS MISSING. LOWER WAS RECOVERED FROM THE RUNWAY. UPPER WHERE ABOUTS STILL UNKNOWN. MANY OF THE CAM LOCK FASTENERS ARE STILL IN PLACE. SOME ARE MISSING AND 1 OR 2 FEMALE SOCKETS ARE NOT DAMAGED.

CA040929001

CNDAIR

GE  

 

ENGINE

INOPERATIVE

9/24/2004

CL6002B19

CF343B1

 

 

NR 2 

(CAN) AT 500 FT THERE WAS A LOUD BANG AND THE NR 2 ENGINE SHUT DOWN, DECLARED AN EMERGENCY. LANDED WITHOUT INCIDENT. ENGINE REPLACED. OVERWEIGHT LANDING INSPECTION ALSO REQUIRED.

CA040615008

CNDAIR

GE  

 

TIRE

SEPARATED

5/27/2004

CL6002B19

CF343B1

 

H29X901516

MLG 

(CAN) NR 2 MLG TIRE SEPARATION/ RUPTURE ENGINE VIBRATION (N1) WAS DEPICTED ON EICAS AND FELT THROUGHOUT THE AIRCRAFT. THE FLIGHT CREW RETARDED THE POWER LEVERS TO REDUCE N1 VIB. TO WITHIN LIMITS. (FYI:AT 42 PERCENT N1 = 3.9 MILS). A/C DIVERTED. FLIGHT CREW POST FLIGHT CHECK WITNESSED 3 FAN BLADES SEVERELY DAMAGED INDUCED BYTHE NR 2 TIRE SEPARATION AND RUPTURE. THE IB FLAP SURFACE HAS SUSTAINED DAMAGE AS WELL. FYI: THIS IS THE SIXTH OCCURRENCE SINCE MAY 11TH, 2004, ASSOCIATED WITH THIS MFG TIRE SEPARATION.

CA040615009

CNDAIR

GE  

 

TIRE

SEPARATED

5/13/2004

CL6002B19

CF343B1

 

H29X901516

MLG 

(CAN) DURING PASSENGER DEPLANING, A RAMPER REPORTED THE LT IB TIRE SHOWN TIRE SEPARATION (TREAD MISSING) AND THE CORD SECTION WAS SHREDDED AND THE TIRE HAD POPED OUT IN SEVERAL AREAS. UPON A CLOSURE LOOK, THE FLIGHT CREW NOTICED THE LT IB FLAP SURFACE HAD SUSTAINED DAMAGED AS WELL. LT NR 1 AND NR 2 TIRES REPLACED. FLAP SURFACE PN 601R14002-1, SN SB/RJ/777 REPLACED. LT ENGINE INSPECTED AND NO DAMAGE WAS FOUND.

CA040802001

CNDAIR

GE  

 

SKIN

LIGHTNING STRIKE

7/30/2004

CL6002B19

CF343B1

 

 

HORIZ STAB

(CAN) THE FLIGHT CERW REPORTED A POSSIBLE LIGHTINING STRIKE , UPON INSPECTION BY MAINTENANCE IT WAS FOUND THAT THERE WAS DAMAGE TO NR 2 DME ANTENNA , NR 2 COMM ANTENNA AND NR 1 AND 2 ATC ANTENNES WHICH WERE REPLACED AND TESTED . ALSO FOUND STRUCTURAL DAMAGE ON RT HORIZONTAL STABLILIZER WHICH WAS REPAIRED IAW MFG EO 601R-55-11-129.

CA040811001

CNDAIR

GE  

 

WINDSHIELD

CRACKED

7/27/2004

CL6002B19

CF343B1

 

NP13932111

COCKPIT

(CAN) CAPTAINS WINDSHIELD SHATTERED, OCCURRED AT FL330, CREW DESCENDED TO FL100, W/S HEAT ON LOW, MFG P: 7.2 WHEN WINDOW SHATTERED. WINDSHIELD REPLACED. (SEE ALSO: US NR 2004081200104)

CA041129001

CNDAIR

GE  

 

WINDOW

CRACKED

11/28/2004

CL6002B19

CF343B1

 

NP1393225

COCKPIT

(CAN) THE LT SIDE WINDOW CRACKED WHILE IN APPROACH. VSB CSB-NP-139322 WAS PERORMED ON NOV 2003. WINDOW WAS REPLACED IAW AMM.

CA040420007

CNDAIR

GE  

 

O-RING

LEAKING

4/15/2004

CL6002B19

CF343B1

 

MS29513326

FUEL COUPLING

(CAN) DURING ROUTINE WALK AROUND , MAINTENANCE DISCOVERED FUEL LEAK AROUND RT WING DRYBAY DRAIN. DRY BAY PANELS WERE REMOVED AND DRY BAY FOUND TO HAVE SMALL AMOUNT OF FUEL PRESENT. THE COUPLING THAT ATTACHES THE AIR SCOOP TO THE FUEL TANK VENTLINES ON THE RT WING WAS FOUND TO BE LEAKING INTO THE DRY BAY. COUPLING PACKINGS WERE REPLACED AND LEAK CHECK WAS COMPLETED WITH NO LEAKS FOUND. AIRCRAFT WAS RETURNED TO SERVICE. AIRCRAFT HOURS WERE 11178:51 AIRCRAFT CYCLES WERE 9107

CA040507002

CNDAIR

GE  

 

SERVO

FAILED

4/23/2004

CL6002B19

CF343B1

 

8220260001

ELEVATOR

DURING CRUISE FLIGHT, AP TRIM IS RWD POSTED ON AND OFF EVERY FEW SECONDS. AUTO-PILOT DISCONNECTED. NOTICED THAT AILERON IS EXTREMELY HARD TO MOVE ALMOST BLOCKED. IN DESCENT WITHOUT AUTO-PILOT, WE NOTICED THAT THE ELEVATOR ALSO COULD NOT BE MOVED (FL310-300 / SAT -50 C). AROUND FL290 AND AFTER APPLYING STRONG INPUT, THE AILERON CAME FREE WITH A JERK. AROUND FL130 (TAT 0C), ELEVATOR FREE AGAIN. APPROACH AND LANDING NORMAL. AILERON AND ELEVATOR SERVO MOUNT CHANGED. OPERATIONAL TESTS ON A/P SERVOS SUCCESSFULLY PERFORMED. AILERON SERVO CYCLE 18126/ HOURS 23075 ELEVATOR SERVO CYCLE 19592/ HOURS 24455.

CA040507001

CNDAIR

LYC  

 

ACTUATOR